These two wells have been removed from the list of wells that need to be followed. They are clearly back on line and are still great wells:
May 19, 2019: on 320-acre spacing; these are the only two wells on this drilling unit; they both went inactive 1/19; remain inactive 3/19:
- 20307, in the west half, A/1,328, EOG, Clarks Creek 103-17H, Antelope, Sanish pool, t11/11; cum 157K 10/19; only 1,000 bbls/month; off line as of 1/19; still inactive, 7/19; 4 days, 8/19; looks to be back on status as of 9/19;
- 19693, in the east half, 722, Enerplus, Danks 17-44H, Antelope, Sanish pool, t7/11; cum 263K 10/19; only 1,000 bbls/month; off line as of 1/19; still inactive, 3/19; active as of 4/19 but only producing one day/month? see this note. And here. Now back up to 4,000 bbls/month with only one day of being on line according to the scout ticket; see this post; strange production profile; again, only one day of production 8/19; only one day of production, 9/19 but produced 3,479 bbls; one day, 10/19, 2,207 bbls;
Recent production for #20307:
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
SANISH | 12-2019 | 24 | 1113 | 1097 | 632 | 1508 | 593 | 598 |
SANISH | 11-2019 | 30 | 1770 | 1797 | 990 | 2422 | 1545 | 469 |
SANISH | 10-2019 | 31 | 2266 | 2264 | 1542 | 3685 | 1504 | 1761 |
SANISH | 9-2019 | 30 | 1654 | 1648 | 1735 | 2327 | 787 | 1132 |
SANISH | 8-2019 | 4 | 6 | 0 | 405 | 71 | 23 | 0 |
SANISH | 7-2019 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
SANISH | 6-2019 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
SANISH | 5-2019 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
SANISH | 4-2019 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
SANISH | 3-2019 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
SANISH | 2-2019 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
SANISH | 1-2019 | 23 | 665 | 611 | 320 | 1331 | 344 | 674 |
SANISH | 12-2018 | 31 | 916 | 953 | 359 | 1920 | 894 | 604 |
SANISH | 11-2018 | 30 | 942 | 962 | 421 | 1794 | 778 | 608 |
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