The most recent well was completed in late 2018/early 2019, and tested 1/19.
Following that completion, this well reported a significant jump in production. Note the small IP, and then note that this well will soon hit 500K; about six years old; jump in production:
- 27068, 502, WPX, Good Voice 34-27HD, Squaw Creek, t11/14; cum 464K 12/19; off line while neighboring wells fracked; off line for about five months; now back on line as of 1/19;
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 12-2019 | 31 | 6442 | 6423 | 2066 | 8742 | 5918 | 1764 |
BAKKEN | 11-2019 | 30 | 6346 | 6479 | 1699 | 8613 | 1082 | 6358 |
BAKKEN | 10-2019 | 31 | 5053 | 5045 | 4923 | 6857 | 1275 | 4539 |
BAKKEN | 9-2019 | 30 | 4878 | 5001 | 3731 | 6619 | 1276 | 4329 |
BAKKEN | 8-2019 | 31 | 4279 | 3970 | 4133 | 5807 | 3205 | 1633 |
BAKKEN | 7-2019 | 18 | 1189 | 1185 | 1072 | 1494 | 629 | 421 |
BAKKEN | 6-2019 | 20 | 1714 | 1728 | 1326 | 2155 | 1439 | 184 |
BAKKEN | 5-2019 | 31 | 3934 | 3914 | 3208 | 4944 | 2875 | 1224 |
BAKKEN | 4-2019 | 30 | 4641 | 4634 | 2711 | 5834 | 2830 | 2106 |
BAKKEN | 3-2019 | 29 | 2840 | 2815 | 347 | 13399 | 12787 | 0 |
BAKKEN | 2-2019 | 28 | 2313 | 2304 | 122 | 11282 | 10743 | 0 |
BAKKEN | 1-2019 | 11 | 1091 | 1085 | 46 | 3481 | 3087 | 0 |
BAKKEN | 12-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 11-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
Off line from late 8/18 to late 1/19.
BAKKEN | 7-2018 | 12 | 1140 | 1184 | 351 | 4486 | 4201 | 0 |
BAKKEN | 6-2018 | 30 | 3069 | 3055 | 797 | 11497 | 10817 | 0 |
BAKKEN | 5-2018 | 31 | 3415 | 3492 | 841 | 10153 | 9420 | 0 |
BAKKEN | 4-2018 | 30 | 3360 | 3278 | 958 | 6622 | 5908 | 0 |
BAKKEN | 3-2018 | 31 | 3822 | 3890 | 871 | 11133 | 10357 | 0 |
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