Thursday, June 21, 2018

Random Update Of Some Older Wells -- June 21, 2018

This well had a nice jump in production in December, 2017, after being off line for about four months; now over 500,000 bbls of oil:
  • 18579, 2,006, Oasis/SM, Jorgenson 1-30H, Bear Den, Bakken, tested 12/10; 120K by 6/11; cum 514K 4/18;
Another MRO well with huge jump in production; noted 8/17:
Monthly Production Data:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
SANISH4-2018305442590215601077183021699
SANISH3-2018316122618118361759016296446
SANISH2-2018287469679427781238157495663
SANISH1-20183188379658317714900315410437
SANISH12-2017319510880135841461291213024
SANISH11-2017301170011524457815178180810712
SANISH10-20171958496142294170941236065
SANISH9-2017301348813450682016223014269
SANISH8-201723120241168394341436016212543
SANISH7-20170000000
SANISH6-20170000000
SANISH5-2017001570000
SANISH4-20172728542886184377703017
SANISH3-20173135113892255462503713

Another well that has gone over 500K bbls cumulative:
Another well that has gone over 500K bbls cumulative:
  • 18924, 1,361, Vixen Federal 1-19-30H, t2/11; Van Hook, Bakken; cum 505K 4/18;
Another well that has gone over 500K bbls cumulative:
  • 18922, 472, WPX/Dakota-3/Zenergy, Skunk Creek 1-12H/Dakota-3 Skunk Creek, South Fork, Bakken, t6/11; cum 545K 4/18;
This well has gone over 650K bbls cumulative: 
  • 18859, 680, CLR, Carson Peak 3-35H, Oakdale, Bakken, t5/11; cum 651K 4/18;
Another well that has gone over 500K bbls cumulative:
  • 18943, 2,169, WLL, Locken 14-9XH, Sanish, Bakken, t11/10; cum 559K 4/18;
Another well that has gone over 500K bbls cumulative:
  • 18546, 3,424, Enerplus, Ethan Hall 6B-31-30-1H, McGregory Buttes, t12/10; cum 537K 4/18; recently went off line; 
A short lateral that has gone over 500K bbls cumulative:
  • 18825, 951, EOG, Van Hook 8-36H, Van Hook, Bakken, single section;100K in 5 months -- whoo-hoo! t7/10; cum 590K 4/18;