Monday, October 3, 2016

Back On Status? An EOG Cottonwood Well That Looked To Be Permanently Plugged Back On Status? -- October 3, 2016

This well:
  • 17850, 487, EOG, Cottonwood 2-35H (1 sec), wells have not been good in this field; Cottonwood, t8/09; cum 132K 9/15; in active as of 9/15; back on status as of 7/16; cum 134K 8/16;
The two most recent sundry forms were received August 3, 2016, and April 29, 2016. Prior to that, one had to go back to the 2009 for information on this well. 

A sundry form received August 3, 2016: workover rig was pulling pipe that had emulsion in it.

A sundry form received April 29, 2016: the well has been shut in for the previous year due to equipment failure. The cost to replace the equipment to bring the well back on production would make the well uneconomical to produce at current oil prices. Company requests a waiver to plug and reclaim an abandoned well....

It should be noted that there are no other "new" wells in this area. This is the only well in this section (35-157-92).

Production profile for past year and a half or so:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN8-201631113012879688876370
BAKKEN7-2016176104307633423420
BAKKEN6-20160000000
BAKKEN5-20160000000
BAKKEN4-20160000000
BAKKEN3-20160000000
BAKKEN2-20160000000
BAKKEN1-20160000000
BAKKEN12-20150000000
BAKKEN11-20150000000
BAKKEN10-20150000000
BAKKEN9-20150000000
BAKKEN8-2015132552032162217047
BAKKEN7-2015315616594625643140
BAKKEN6-2015305415254635412990
BAKKEN5-2015315436646926183680
BAKKEN4-2015305125454465423000

Production profile for first six months:
BAKKEN1-201031532854773148389103736
BAKKEN12-200929426742202704313802994
BAKKEN11-200915308231272179225402183
BAKKEN10-200922425141832665311803008
BAKKEN9-200930686168785846502804878
BAKKEN8-200911402933486723274502690

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