This well was drilled in 1993. a vertical, non-Bakken well. Note the jump in production in May, 2022. Actually the production jump began a month earlier, in April, 2022, but was taken off line due to the April blizzard. The 7,976 bbls over nineteen days in April extrapolates to 12,594 bbls over 30 days. Pretty good for a vertical well drilled 29 years ago.
See if you notice something else interesting about this well.
The well:
- 13447, 419, ConocoPhilips, Dickinson-Lodgepole Unit 74, Dickinson, t2/93; F; cum 3.215588 million 8/19; cum 3.32 million bbls 5/22;
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
LODGEPOLE | 5-2022 | 31 | 8674 | 8643 | 23496 | 5929 | 5929 | 0 |
LODGEPOLE | 4-2022 | 19 | 7976 | 7838 | 9922 | 4128 | 4128 | 0 |
LODGEPOLE | 3-2022 | 4 | 398 | 423 | 1859 | 102 | 102 | 0 |
LODGEPOLE | 2-2022 | 24 | 2211 | 2287 | 11758 | 815 | 815 | 0 |
LODGEPOLE | 1-2022 | 30 | 2748 | 2680 | 13808 | 1028 | 1028 | 0 |
LODGEPOLE | 12-2021 | 30 | 2559 | 2551 | 15738 | 1120 | 1120 | 0 |
LODGEPOLE | 11-2021 | 29 | 2433 | 2440 | 16130 | 1224 | 1224 | 0 |
LODGEPOLE | 10-2021 | 30 | 2763 | 2762 | 17459 | 1473 | 1473 | 0 |
LODGEPOLE | 9-2021 | 29 | 2543 | 2543 | 18836 | 1308 | 1308 | 0 |
LODGEPOLE | 8-2021 | 30 | 2392 | 2439 | 19719 | 1341 | 1341 | 0 |
LODGEPOLE | 7-2021 | 30 | 2530 | 2484 | 21701 | 1605 | 1605 | 0 |
No comments:
Post a Comment
Note: Only a member of this blog may post a comment.