A reader suggested that I note that not all Bakken wells are as good as this one.
The well:
- 16902, 2,192, Whiting, Lacey 11-1H, Sanish, t7/08; cum 521K 12/20; one of the few wells that did not go off line, 5/20; just went off line 7/21; cum 522K 6/21; see this post; off line 8/21; remains off line 10/21; cum 540K 5/22;
- how did this happen (see production profile below): now look at this well on that pad that was just fracked -- link here:
Recent production:
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 5-2022 | 31 | 2754 | 2854 | 1134 | 1693 | 1631 | 0 |
BAKKEN | 4-2022 | 28 | 2566 | 2484 | 704 | 1579 | 1386 | 137 |
BAKKEN | 3-2022 | 31 | 2663 | 2698 | 1200 | 927 | 865 | 0 |
BAKKEN | 2-2022 | 28 | 2467 | 2491 | 957 | 923 | 821 | 46 |
BAKKEN | 1-2022 | 31 | 2951 | 2989 | 1161 | 1441 | 1379 | 0 |
BAKKEN | 12-2021 | 31 | 2881 | 2740 | 1486 | 1645 | 1583 | 0 |
BAKKEN | 11-2021 | 30 | 930 | 888 | 569 | 599 | 540 | 0 |
BAKKEN | 10-2021 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 9-2021 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 8-2021 | 1 | 0 | 0 | 3 | 0 | 0 | 0 |
BAKKEN | 7-2021 | 20 | 276 | 299 | 81 | 300 | 291 | 9 |
BAKKEN | 6-2021 | 25 | 321 | 330 | 172 | 436 | 409 | 27 |
BAKKEN | 5-2021 | 31 | 325 | 340 | 93 | 307 | 307 | 0 |
BAKKEN | 4-2021 | 24 | 383 | 330 | 116 | 616 | 616 | 0 |
BAKKEN | 3-2021 | 1 | 7 | 58 | 2 | 10 | 10 | 0 |
No comments:
Post a Comment
Note: Only a member of this blog may post a comment.