Saturday, December 28, 2019

The Bakken -- Simply Staggering -- December 28, 2019

Do you remember this well?
  • 31774, 5,058, Bruin, Fort Berthold 151-94-27A-34-16H, API: 33-053-07183, Antelope-Sanish; a staggering well; 55 stages; 14.4 million lbs according to operator; t7/18; cum 516K 10/19;
Full production profile:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
SANISH10-2019134670482481741272389511512
SANISH9-20193011737116801199443185300927419
SANISH8-20192612237122557087360912020412153
SANISH7-20193116026163908787570772108330054
SANISH6-2019301486914784920426380894512951
SANISH5-201931200841991712724490002495419430
SANISH4-201930240522414613698415422046015790
SANISH3-2019121074610450650423783153725897
SANISH2-20192826631272522405558158465826886
SANISH1-201930309373064220592707625395311816
SANISH12-201831502425019426772879655842429261
SANISH11-201819237182370116934277531503012602
SANISH10-201831622856223355956864285612330017
SANISH9-201830503575088155448689445338015111
SANISH8-201831960459618370073925397253819688
SANISH7-201822612346033883791824931667665537

The graphic:


Wells of interest (note: two wells went over 500,000K cumulative):
  • 22707, 1,959, Bruin, Fort Berthold 151-94-26B-35-3H, Antelope-Sanish, t4/14; cum 588K 10/19; with jump in production, 4/19;
  • 22708, 1,776, Bruin, Fort Berthold 151-94-26B-35-2H, Antelope-Sanish, t4/14; cum 353K 10/19; with jump in production, 5/19;
  • 20328, 1,647, Bruin, Fort Berthold 151-94-26B-35-1H, Antelope-Sanish, t3/12; cum 570K 10/19; no jump in production;

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