Tuesday, November 5, 2019

This Well Is Simply Staggering -- But Not Particularly Unusual For A Bakken Well -- November 5, 2019

The dreaded Bakken decline? 

Disclaimer: I am inappropriately exuberant about the Bakken. 

This page will not be updated.

This well's cumulative production has just had a huge jump -- this well is now approaching 600,000 bbls cumulative -- was drilled as recently as 2015.

The well:
  • 29867, 3,126, BR, Kirkland 14-21TFH, ULW, Pershing, will be shut-in for the reason that the gathering line infrastructure to connect the well does not exist and/or has not been built at this location yet; this well has not been completed and it will be shut-in until the infrastructure is built; t10/15; cum 581K 9/19;
Recent production:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN9-201930154451551589711836588639428
BAKKEN8-2019311653416466902822311134078827
BAKKEN7-2019311276112956879416469451711875
BAKKEN6-20193017228173319023304391246317902
BAKKEN5-201931221652202111560379902410613807
BAKKEN4-20193022438225161274439734357333927
BAKKEN3-20193123614239591490141265397301458
BAKKEN2-2019281872518620984822838227680
BAKKEN1-20193117742174841140225314211554082
BAKKEN12-20183116062161641098922063195582428

Production when this well was first drilled/completed back in 2015:
BAKKEN9-2016301867518677498030904308180
BAKKEN8-2016312158721571484732913328250
BAKKEN7-2016312356323584540334640345510
BAKKEN6-2016292089820789541329137291230
BAKKEN5-2016311273212767493824528245140
BAKKEN4-201630165931660526023073230600
BAKKEN3-2016311585515807406721817218020
BAKKEN2-201620106101067029011474914538199
BAKKEN1-2016312515125052497326375263600
BAKKEN12-201525865332169479450
BAKKEN11-20150000000
BAKKEN10-201581404114041675722719022699

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