Tuesday, November 5, 2019

Random Update Of Just A Few Wells Drilled/Completed Back In 2010 That Have Gone Over 500K Bbls Cumulative -- November 5, 2019

The wells:
  • 18232, 860, Nichols 10-15H (Hunt), Ross, t1/10; cum 502K 9/19;
  • 18238, 323, Grace 2-11H (Murex), t12/09; cum 527K 9/19;
  • 18209, 1,380, Thomas Patrick 1-12H (Murex), Sanish, t11/09; cum 637K 9/19; 
  • 18298, IA/3,422, Kannianen 44-33H (Whiting); t1/10; cum 701K 4/19; off line since 4/19; 
  • 17080, 2,096, Niemi 44-22H, (Whiting), Sanish; t10/09; cum 526K 9/19;
  • 18213, 3,308, Whiting, Platt 44-28H (Whiting), Sanish , t12/09; cum 567K 9/19;
  •  18190, 463, Armstrong, Laurine Engel 1, conventional, Dickinson, Lodgepole; 61,000 barrels in first five months (at $60 = $3.6 million and this is a conventional well); cum 880K 9/19;
  • 17122, 581, EOG,  Austin 23-32H, 1 sec, Parshall (90,000 bbls in 135 days); t8/09; cum 675K 9/19;
  • 17841, 602, Murex, Clifford Gene 1-12H, 2 sec, Sanish (144K bbls/first 7 months) (don't confuse this with the Gene 1-22H which is operated by Samson - #18009 -- being drilled in February, 2010; off confidential list in July, 2010); t5/09; cum 675K 9/19; (taken off-line in summer, 2012; back on line in 2013) 
  • 18209, 1,380, Murex, Thomas Patrick 1-12H, 2 sec, Sanish (89K bbls/first 91 days), first reported Feb 1, 2010; t11/09; cum 637K 9/19;
  • 18180, 2,561, Slawson, Stallion 1-1-12H, Big Bend (I forgot to report this one earlier in month); t2/10; cum 518K 9/19; 
  • 18109, IA/2,409, Whiting, Tollefson 44-10H, 2 sec, 84k in 108 days, Sanish, t9/09; cum 669K 4/19; off line since 4/19;
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Sophia, age 5, in her "Strikers" soccer uniform.

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