Pay attention to these wells:
- #20521 drilled back in 2012.
- #17407 drilled back in 2009.
- The 31XXX wells completed in July, 2018.
Pertinent production for #20521. This well has not produced since 2015 when it was producing 2,000 bbls / month. Came off-line when Saudi Surge destroyed oil prices. Operator managing assets very, very well:
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 7-2018 | 25 | 10219 | 9853 | 25037 | 13195 | 0 | 13168 |
BAKKEN | 6-2018 | 2 | 0 | 0 | 2229 | 0 | 0 | 0 |
BAKKEN | 5-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 4-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 3-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 2-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 1-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
So, how is #31966, one of the 31XXX wells looking?
- 31966, 1,803, XTO, George Federal 21X-19F2, Lost Bridge, t7/18; cum 18K after 20 days; 2nd bench of the Three Forks --
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 7-2018 | 20 | 18482 | 17820 | 46026 | 20147 | 0 | 20105 |
BAKKEN | 6-2018 | 1 | 0 | 0 | 3970 | 0 | 0 | 0 |
Other wells:
- 31964, 2,823, XTO, George Federal 21X-19E, Lost Bridge, t7/18; cum 16K after 8 days, extrapolates to 60,000 bbls for a 30-day month.
- 31961, SI/NC, XTO, Bang Federal 21X-19A, Lost Bridge, t--; cum 15K after 11 days;
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Screen Test For A New David Lynch Movie
Taken some years ago.
No, she did not get the part. Apparently David felt she was "over-acting."
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