- 32029, 1,258, Hess, EN-Pederson-LW-154-94-0408H-5, Alkali Creek, 4-section spacing; sections 4,5,8, and 9; t1/16; Three Forks, 50 stages, 3.5 million lbs; cum 79K 4/16; API: 33-061-03842;
- 32030, 917, Hess, EN-Pederson-LW-154-94-0408H-6, Alkali Creek, 4-section spacing; sections 4,5,8, and 9, a middle Bakken well; 35 stages, 2.5 million lbs; t2/16; cum 38K 4/16;
- 32031, 1,275, Hess, EN-Pederson-LW-154-94-0408H-7, Alkali Creek, 4-section spacing; sections 4,5,8, and 9, Three Forks, 50 stages, 3.5 million lbs; t2/16; cum 63K 4/16;
- 32032, SI/NC, Hess, EN-Pederson-LW-154-94-0408H-8, Alkali Creek, 4-section spacing; sections 4,5,8, and 9;
****************************
End Of The Road For This Well
After following this well for quite some time through a complicated course, it looks like the company has cut their losses, and capped and buried this well, calling it a dry well. I began following it on August 19, 2014:
August 19, 2014, waiting for frack data to see where this horizontal ended up:
- 27209, dry, Petro-Hunt, USA 153-95-4B-9-2HR, Charlson, Three Forks B2, sections 4, 5, 8, 9 - 153-95; TVD, 9,978; TD, 19,839; 2560-acre spacing; azimuth 214 degrees; orig app permit name: USA 153-95-4B-9-1HS, February 14, 2014: request rec'd to change well to be under spacing order #22895, 1280-acre spacing; so I believe the "R" is a revised request/permit to change from 2560-acre spacing to 1280-acre spacing; same date, request rec'd to change name to "2HR" -- same target; it looks like TD was reached at a measured depth (MD) of 8,767 feet on March 18, 2014; in limestone; depths, prognosis: Lodgepole - 9,061; Bakken Shale - 9,767; Middle Bakken - 9,791; Target Horizon - 9,814; geology report said this was a Middle Bakken well; frack data not yet posted; [Updates: 7/15 -- still on DRL status;] API 33-053-05540.
- This is a complicated well; from the geologic summary: the initial phase of this well was to be an intersection well intended to intersect the USA 153-95-4B-9-2H (#26446 -- DRY, cease drilling, February 14, 2014; circulation was lost at 8,540 feet an the well was abandoned) vertical in order to cement and plug the well beneath the surface where it packed off. Then a sidetrack out of the cement to drill a vertical and curve, landing thirty feet into the middle Bakken formation. This well spudded February 19, 2014, and reached a TD of 8,768 feet MD on March 18, 2014.
- The well was abandoned and plans are to ski the rig and intersect the wellbore and plug it shut, then sidetrack and re-drill the well.
No comments:
Post a Comment
Note: Only a member of this blog may post a comment.