Locator: 48373B.
This well, originally drilled back in 2009, went from inactive to abandoned back to active -- again, completely "destroying" Hubbert's peak oil theory -- at least as far as occurring in my investing lifetime.
The well:
- 17612, A/AB/IA/4,345, Whiting, Maki 11-27H, Sanish, t10/09; cum 882K 11/19; off line 12/19; remains off line 12/20; remains off line 10/22; cum 886K 2/23; cum 906K 10/24;
It was abandoned back in late 2019, producing 1,000 bbls / month. It remained off line from 12/2019 to 12/22 -- almost exactly three years, and then brought back on line, still producing over 1,000 bbls month:
AKKEN | 4-2023 | 30 | 979 | 1012 | 1973 | 2204 | 2114 | 32 |
BAKKEN | 3-2023 | 31 | 1595 | 1586 | 609 | 3288 | 3122 | 104 |
BAKKEN | 2-2023 | 27 | 1535 | 1497 | 312 | 2084 | 2030 | 0 |
BAKKEN | 1-2023 | 26 | 1123 | 1116 | 377 | 1664 | 1606 | 6 |
BAKKEN | 12-2022 | 29 | 1001 | 990 | 133 | 3518 | 3301 | 161 |
BAKKEN | 11-2022 | 2 | 55 | 53 | 5 | 242 | 239 | 0 |
BAKKEN | 10-2022 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 9-2022 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 8-2022 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 7-2022 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 6-2022 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 5-2022 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 4-2022 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 3-2022 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 2-2022 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 1-2022 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 12-2021 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
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