Monday, March 2, 2020

Oasis Reports A Nice Kellogg Federal Well — Monday, March 2, 2020

Active rigs:

$48.043/2/202003/02/201903/02/201803/02/201703/02/2016
Active Rigs5267594134

Only two wells came off the confidential list today:
  • Sunday, March 1, 2020: 1 for the month; 172 for the quarter, 172 for the year:
    • 35251, 655, Oasis, Kellogg Federal 5297 44-19 13BX, middle Bakken, 40 stages; 8 million lbs; Banks, t9/19; cum 146K 1/20; see below;
  • Saturday, February 29, 2020: 64 for the month; 171 for the quarter, 171 for the year:
    • 32461, drl, Sinclair Oil, Crosby Creek 4-5H, Little Knife, no production data;
#35215:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN1-20203141669416351401811617010456310925
BAKKEN12-20193131586317251247783200807031815
BAKKEN11-201930372023747215587906917042519606
BAKKEN10-20193131900318891599172658663595617
BAKKEN9-2019533942852111783036856787
BAKKEN8-20190000000
  
From the well file for #35215:
  • sixteen miles northeast of Watford City
  • surface hole drilled prior to Nabors B01's arrival
  • surface casing was set / cemented to 2,260'
  • re-entered on March 31, 2019; reached TD of 10,490 using two separate BHA
  • the curve was drilled in 8.67 hours, using a single BHA
  • the lateral was drilled using a single BHA
    • lateral was drill in a total of three days
    • exposed 9,918' of uncased hole, entirely within the middle Bakken member;
    • reached TD of 21,190' MD on April 7, 2019 (seven days total drilling)
  • middle Bakken: 
    • entered at 11,201' MD; 10,965' TVD
    • the target was18' thick; beginning 11' below the base of the upper Bakken shale and extending to 11' above the lower Bakken shale
  • gas shows:
    • vertical: max at 875 units
    • lateral: from 150 to 3,000 units, averaging around 1,500 units
    • background gases showed increased in magnitude significantly gradually throughout the lateral;

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