Tuesday, October 29, 2019

Random Update Of An Older Well Returned To Production After Neighboring Wells Fracked -- October 29, 2019

This page won't be updated.

These two wells came off confidential well today:
  • 35282, 1,515, Enerplus, Blackberry 149-93-21B-22H, this well is tracked here; Mandaree, t4/19; cum 101K 8/19;(#22748 with jump in production)
  • 35281, 1,401, Enerplus, Boxwood 149-93-21B-22H-TF, this well is tracked here; Mandaree, t4/19; cum 78K 8/19;
An older well in the immediate area:
  • 22748, 729, Enerplus, Chokecherry 149-93-21A-22H, Mandaree, t11/12; cum 247K 8/19;
Note: this well was originally drilled back in 2012. Note recent production:

PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN8-201931424143214056333132450
BAKKEN7-201924642864018251450025341898
BAKKEN6-20193091209043542863846081211
BAKKEN5-2019623772567629516641332314
BAKKEN4-20190000000
BAKKEN3-20190000000
BAKKEN2-20190000000
BAKKEN1-2019112624483931830136
BAKKEN12-2018311553151210911088640315
BAKKEN11-201825145414469991018183768
 

No comments:

Post a Comment

Note: Only a member of this blog may post a comment.