Wednesday, June 5, 2019

Random Update Of WPX Well In Spotted Horn After Neighboring Well Fracked -- June, 5, 109

This well showed significant increase in production after a neighboring wells was fracked:
  • 29445, 2,441, WPX, Emma Owner 23-14HB, Spotted Horn, t3/16; cum 495K 4/19; see production profile below;
The neighboring well that was fracked:
  • 34648, 2,498, WPX, Lead Woman 23-14HQ, Spotted Horn,  t12/18; cum 168K 4/19;
Production data of relevance:
  • 29445:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN4-2019301284812942103081737114603926
BAKKEN3-20193114060139951180519009145712452
BAKKEN2-20192811256113211126515219117221862
BAKKEN1-20192391329036108811234738157125
BAKKEN12-20183118159181872944524550658615551
BAKKEN11-2018417981727224524311206726
BAKKEN10-201817304530892000411618861513
BAKKEN9-20181320092039116327171562604
BAKKEN8-201831500049392380676039841789
BAKKEN7-201831539354412053729245051738

  • The Lead Woman well, #34648, had 50K+ production:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN4-2019181703216974928620150168031201
BAKKEN3-201931242192418817978286511085114667
BAKKEN2-2019282772027746214463279428628710
BAKKEN1-20193128389283712840037379338010
BAKKEN12-201831555395567843018657032500634212
BAKKEN11-20182615404150482450618223570110874

No comments:

Post a Comment