From Energent Group:
Kraken Operating completes multiple 60 stage wells in Williston (2019-01-24) and (2019-02-01)
The Pocasset LW 32-29 #1H was drilled to a measured depth of 21,210 ft and perforated from 10,983 to 21,138 ft. It flowed 1,105 bbl of oil, 1,156 MMcf of gas, and 2,135 on its January 27 test date. The 32-29 #1H was stimulated November 12 with a max PSI of 9,143 and a max rate of 83.1.
The Pocasset 32-29 #6TFH produced 892 bbl of oil, 759 MMcf of gas, and 2,825 bbl of water February 5. It was stimulated November 28 with a max PSI of 9,317 and a max rate of 87.7.
The Pocasset 32-29 #7H was drilled to a measured depth of 21,221 ft and produced 1,183 bbl of oil, 502 MMcf of gas, and 2,264 bbl of water. Kraken reported a stimulation November 27 with a max PSI of 9,497 and a max rate of 89.6.
From the blog back on March 15, 2019; February 27, 2019; February 22, 2019:
- 35328, 1,105, Kraken, Pocasset LW 32-29 1H, Oliver, t1/19; cum --;
- 35327, 737, Kraken, Pocasset 32-29 4TFH, Oliver, t1/19; cum --;
- 35326, 944, Kraken, Pocasset 32-29 5H, Oliver, t2/19; cum --;
- 35325, 892, Kraken, Pocasset 32-29 6TFH, Oliver, t2/19; cum --;
- 35324, 1,183, Kraken, Pocasset 32-29 7H, Oliver, t2/19; cum --;
- 34893, 1,226, Pocasset 29-32 2H, Oliver, t2/19; cum --;
- 34894, 1,290, Pocasset 29-32 3TFH, Oliver, t2/19; cum --;
- Neighboring well, #24013, with nice jump in production
- #23705, also taken off line is now just being returned to production (2/19)
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