The Enerplus Tailor Pad in Mandaree Oil Field -- March 28, 2019
The three Enerplus wells that came off confidential list today:
- 34416, 1,086, Enerplus, Scissors 149-93-04B-03H, 33-025-03421, 34 stages; 8.2 million lbs, Mandaree, t10/18; cum 83K 1/19; total drilling days, 18; total drilling hours, 109.4 hours; a strong gas show of 4,981 units while drilling the Lodgepole; the well landed an estimated 25 feet into the middle Bakken; the target was the "Clean B" and appeared somewhat thicker than prognosis; no trips in the lateral; connection gases built to hte 3,300 to 5,000 unit range after 17,500' MD; a 20' flare noted.
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
BAKKEN | 1-2019 | 31 | 18521 | 18585 | 15685 | 18521 | 13023 | 3749 |
BAKKEN | 12-2018 | 24 | 17744 | 17498 | 14802 | 17744 | 8333 | 8446 |
BAKKEN | 11-2018 | 24 | 18375 | 18677 | 14948 | 18375 | 9822 | 8123 |
BAKKEN | 10-2018 | 30 | 27582 | 27539 | 35325 | 27582 | 6068 | 20984 |
BAKKEN | 9-2018 | 3 | 998 | 375 | 1106 | 998 | 552 | 405 |
- 34415, 1,490, Enerplus, Thimble 149-93-04B-03H, 33-025-03420, 34 stages; 11.9 million lbs, Mandaree, t10/18; cum 113K 1/19; drilling days, 17; drilling hours, 122.3; target: middle Bakken C Zone; Stoneham Rig 18 walked form the Thimble 149 well to this location on June 25, 2018; no trips in the lateral; much lower gas than Scissors but at 21,184' MD gas was over 3,400 units with a 10 - 15' flare.
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
BAKKEN | 1-2019 | 17 | 15390 | 15803 | 12688 | 15390 | 11074 | 3472 |
BAKKEN | 12-2018 | 31 | 25475 | 25187 | 19573 | 25475 | 11994 | 11758 |
BAKKEN | 11-2018 | 29 | 29844 | 30254 | 23547 | 29844 | 15910 | 13178 |
BAKKEN | 10-2018 | 30 | 42213 | 41376 | 63534 | 42213 | 9117 | 32373 |
BAKKEN | 9-2018 | 3 | 264 | 99 | 4416 | 264 | 146 | 102 |
- 34414, 1,450, Enerplus Tailor 149-93-04B-03H-TF, 33-025-03419, 34 stages; 10.2 million lbs, Mandaree, t10/18; cum 73K 1/19; total days drilling, 24; total drilling hours, 114.9; drilling the lateral, an intermittent 2' - 1' flare was established; connection gases built to 3,500 - 4,000 units by 11,000' MD; flare became more consistent after 17,500'. No trips in the lateral. Trip gas after the short trip at TD of 21,224' MD was only 1,400 units with a 4' flare.
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
BAKKEN | 1-2019 | 20 | 8620 | 8953 | 9569 | 8620 | 6273 | 1728 |
BAKKEN | 12-2018 | 31 | 17376 | 17084 | 17036 | 17376 | 8135 | 7992 |
BAKKEN | 11-2018 | 27 | 15122 | 15562 | 17127 | 15123 | 8184 | 6514 |
BAKKEN | 10-2018 | 30 | 30319 | 30723 | 40331 | 30320 | 6770 | 22974 |
BAKKEN | 9-2018 | 2 | 1838 | 690 | 8865 | 1839 | 1016 | 776 |
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