Comments/Updates
Comments that came in later, for newbies:
- for minimal cost, MRO seems to have gotten a brand new well
- MRO was pretty much guaranteed a brand new well -- something we never saw before the "unconventional" drilling / "the shale revolution"
- the company did not have to pay upfront costs for a new lease; did not have to negotiate with the surface owner; is not paying additional surface "rent"; did not have to build a new pad; did not have to pay for new infrastructure, including new electricity access (a big choke point during the boom);
- every well drilled before 2016 is a candidate for a re-frack
- by the time every well drilled before 2016 is re-fracked, it will be time to re-frack all the wells drilled between 2016 and 2022
- when the Bakken boom began, primary production was estimated to be 1 - 3%
- no one is talking but tea leaves suggest primary production in the Bakken is now in the low teens
- conventional drilling, primary production, 50%?
- can't wait to see EUR-type curves coming out of the Bakken in 2025
Original Post
Art Berman, put #17255 in your pipe and smoke it.
First this well:
- 17255, 465/1,799, MRO, Pelton 24-31H, Bailey, t9/08 and 4/17;
- from the sundry form, dated March 1, 2017: MRO is planning to refrack this well. Originally an open hole completion in 2008 and drilled with toe setbacks that were 500' FNL of section 30. This well had an original TD depth of 19,932' MD. MRO plans to put a rig on this well, extend the lateral starting at a tie-on survey at approximately 19,885' MD,and drill an approximate additional 450' of lateral (extending lateral to approximately 160' FNL of section 30). MRO will then run a cemented liner for a 45-stage plug and perf style completion.
- second frack: 45 stages; 5.2 million lbs; cum 502K 4/29; full production profile here; recent production data. :
BAKKEN | 9-2017 | 30 | 16370 | 16300 | 12276 | 12112 | 4158 | 6024 |
BAKKEN | 8-2017 | 31 | 20279 | 20304 | 16384 | 14979 | 5244 | 7381 |
BAKKEN | 7-2017 | 31 | 25626 | 25591 | 25477 | 18929 | 1475 | 14540 |
BAKKEN | 6-2017 | 24 | 18177 | 18187 | 19613 | 13250 | 3910 | 7265 |
BAKKEN | 5-2017 | 31 | 23337 | 23366 | 28948 | 17072 | 10811 | 3582 |
BAKKEN | 4-2017 | 7 | 8727 | 8599 | 215 | 6256 | 1976 | 3308 |
BAKKEN | 3-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 2-2017 | 8 | 202 | 184 | 40 | 163 | 93 | 4 |
BAKKEN | 1-2017 | 31 | 896 | 875 | 207 | 688 | 317 | 96 |
BAKKEN | 12-2016 | 29 | 771 | 756 | 187 | 608 | 347 | 11 |
BAKKEN | 11-2016 | 30 | 834 | 865 | 192 | 643 | 365 | 9 |
BAKKEN | 10-2016 | 31 | 863 | 842 | 206 | 681 | 402 | 1 |
Now we have another nice MRO in that very same drilling unit that has come off-line:
- 22333, IA/1,086, MRO, RH 34-31TFH, t9/12; cum 190K 4/20; off-line 5/18; back on line 5/19;
NDIC File No: 22333 API No: 33-025-01608-00-00 CTB No: 222332
Well Type: OG Well Status: IA Status Date: 8/15/2018 Wellbore type: Horizontal Location: SWSE 31-146-93 Footages: 293 FSL 2321 FEL Latitude: 47.416327 Longitude: -102.576085 Current Operator: MARATHON OIL COMPANY Current Well Name: RH 34-31TFH Elevation(s): 2290 KB 2265 GR 2265 GL Total Depth: 20492 Field: BAILEY Spud Date(s): 6/1/2012 Casing String(s): 9.625" 2091' 7" 10939' Completion Data Pool: BAKKEN Perfs: 11275-20492 Comp: 9/6/2012 Status: AL Date: 12/21/2012 Spacing: 2SEC Cumulative Production Data Pool: BAKKEN Cum Oil: 171158 Cum MCF Gas: 120288 Cum Water: 154425 Production Test Data IP Test Date: 9/6/2012 Pool: BAKKEN IP Oil: 1086 IP MCF: 882 IP Water: 1597 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Monthly Production Data
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