A million-bbl EOG Austin well, 21-28H, #17227, short lateral went off line 7/18; no neighboring activity noted; nothing in the sundry forms;
Slawson Whitmore wells in Parshall oil field recently fracked, #34921 and #34922. Not sure which way they are running, but based on name and fact that another Whitmore well is off line, it suggests the wells are running north; sited in an unusual location if that's accurate; #17303, a Whitmore well to the north, off-line; two EOG Austin wells (#25839, #25840) in the same area are also off line. Also note this incredible Slawson Whitmore well, drilled in 2008, that went off line 7/18:
- 17354, 2,205, Slawson, Whitmore 1-7H, Parshall, short lateral, t10/108; cum 656K 10/18;
- 17318, 483, MRO, Clive Pelton 34-23H, Bailey, t8/08; cum 178K 5/18; taken off-line mid-4/18;
- 17345, 902, Newfield, Wisness 1-4H, Westberg, t3/09; cum 428K 10/18; taken off line for less than a month, off and on prior to the jump in production/
- 17319, 329, BR, CCU Audubon 41-27H, Corral Creek, t12/08; cum 282K 10/18; FracFocus, no re-frack; recent frack:
- 29068, 73, BR, CCU Boxcar 34-22TFH, Corral Creek, t3/18; cum 112K 9/18; [#17319]
BAKKEN | 9-2018 | 30 | 6252 | 6758 | 2683 | 2946 | 2872 | 0 |
BAKKEN | 8-2018 | 29 | 5148 | 4598 | 3746 | 2918 | 2846 | 0 |
BAKKEN | 7-2018 | 22 | 3379 | 3360 | 3031 | 1553 | 1498 | 0 |
BAKKEN | 6-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 5-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 4-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 3-2018 | 1 | 48 | 0 | 0 | 2 | 0 | 0 |
BAKKEN | 2-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 1-2018 | 4 | 25 | 0 | 23 | 20 | 10 | 0 |
BAKKEN | 12-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 11-2017 | 4 | 190 | 465 | 30 | 117 | 107 | 0 |
BAKKEN | 10-2017 | 31 | 1437 | 1375 | 260 | 1098 | 1021 | 0 |
BAKKEN | 9-2017 | 30 | 1320 | 1132 | 244 | 1142 | 1068 | 0 |
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