Tuesday, May 1, 2018

Random Update Of A WPX Well With A Nice Jump In Production -- May 1, 2018

I've been following this well for quite some time.
  • 19973, 141, WPX. Wolf 27-34H, Squaw Creek, t7/11; cum 275K 3/18; 
I first got interested in this well on September 17, 2017, and then continued to follow it, and posted updates:
  • September 17, 2017: #19973, neighboring wells fracked 6/17; this well taken off-line 6/17; WPX, Rachel Wolf, Squaw Creek; updated October 19, 2017; huge wells; halo effect. See how long halo affect lasts. Still obvious 12/17; looks like halo effect still as of 1/18 - but only 11 days of production in 1/18; only 10 days in 2/18;
But now, 3/18, back up to 10,269 bbls in one month:

PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN3-2018311026910546613717838126993417
BAKKEN2-201810266725611441463311643001
BAKKEN1-20181137243658185564806075352
BAKKEN12-2017316820660164171184852545231
BAKKEN11-2017306405644274521112457474080
BAKKEN10-2017318714870891571513679975574
BAKKEN9-20173085048631138021477176965553
BAKKEN8-2017203026290110314525627361948
BAKKEN7-20171201404
BAKKEN6-20172089195841715481013121
BAKKEN5-2017311376130763923891467151

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