Random Update Of An MRO Trotter Well That Was Re-Fracked -- November 11, 2017
September 25, 2017: 16875,
MRO, re-fracked:
- 16875, 351, MRO, Trotter 14-23H, Bailey, t2/08; cum 260K 9/17; re-fracked 6/17;
Recent monthly production data:
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
BAKKEN | 9-2017 | 30 | 15426 | 15439 | 11041 | 11920 | 9872 | 221 |
BAKKEN | 8-2017 | 31 | 22205 | 22187 | 20434 | 15952 | 7119 | 6273 |
BAKKEN | 7-2017 | 28 | 18594 | 18579 | 16611 | 24146 | 7538 | 14463 |
BAKKEN | 6-2017 | 3 | 265 | 0 | 1 | 345 | 0 | 316 |
BAKKEN | 5-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 4-2017 | 0 | 0 | 0 | 0 | 0 | 0 |
|
The refrack produced results much, much better than the original frack:
BAKKEN | 9-2008 | 30 | 1989 | 2067 | 368 | 1230 | 1230 | 0 |
BAKKEN | 8-2008 | 31 | 2348 | 2281 | 471 | 1487 | 1487 | 0 |
BAKKEN | 7-2008 | 31 | 2622 | 2669 | 556 | 1444 | 1444 | 0 |
BAKKEN | 6-2008 | 30 | 3102 | 3336 | 649 | 1613 | 1613 | 0 |
BAKKEN | 5-2008 | 31 | 3683 | 3469 | 886 | 1793 | 1793 | 0 |
BAKKEN | 4-2008 | 30 | 4536 | 4630 | 1018 | 2497 | 2497 | 0 |
BAKKEN | 3-2008 | 31 | 5953 | 6063 | 1381 | 1077 | 1077 | 0 |
BAKKEN | 2-2008 | 26 | 7566 | 6983 | 2392 | 0 | 0 | 0 |
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