Wednesday, April 6, 2016

Update On #20336: BR Drilling New Lateral From Existing Site/Well -- April 6, 2016

Updates 

November 23, 2016: huge update here for #20336.

Original Post
Posted earlier:
  • 30774, see above, Whiting, Flatland Federal 22-4-5TFH, Twin Valley:
DateOil RunsMCF Sold
2-201643447108095
1-201654271132061
12-201563835147947
11-20153495349686
10-20151679630293

A graphic of the area:


I didn't spend a lot of time looking, but it appears there was no evidence of any halo effect. However, the index well was a Three Forks well, and the existing, neighboring wells were middle Bakken wells.

Note, #20336: BR is drilling another later from this same location; rig on-site. The bottom hole location will be about 200 feet north of the existing bottom hole location. It will be renamed: Sun Notch 43-32H-R.

From an October 28, 2015, posting, with updates:

A Burlington Resources well was permitted for re-entry:
  • 20336, re-entry/1,162, BR, Sun Notch 43-32H-R/Sun Notch 43-32H, Sand Creek, McKenzie County, 20 stages, 2.1 million lbs; target zone, 20-feet; ; t9/11; cum 41K 2/16;
Comments:   
  • I track the Sand Creek oil field here;  
  • of interest, this well, #20336, was the very first permit I posted following the original post, back in 2011
  • note: this well is still listed as having no pump; on "F" status 
  • note: this well's status is now LOC;
  • there is nothing in the file report that suggests there was any specific problem with drilling or fracking and yet this is a very, very poor well
  • it was originally fracked with 20 stages; 2.1 million lbs proppant
  • I assume they are going back into re-frack, possibly target a different zone, but I don't think a permit is needed for simple "re-working" (although I don't know)
  • I will track this well at "things to follow up on" 
  • this is getting way in the weeds, but maybe an interesting poll question to come out of this one 
NDIC File No: 20336    
Well Type: OG     Well Status: A     Status Date: 9/18/2011     Wellbore type: Horizontal
Location: NESE 32-153-96     Footages: 1320 FSL 275 FEL
Latitude: 48.027371     Longitude: -103.044524
Current Operator: BURLINGTON RESOURCES OIL & GAS COMPANY LP
Current Well Name: SUN NOTCH 43-32H
Elevation(s): 2378 KB   2352 GR   2352 GL     Total Depth: 20457     Field: SAND CREEK
Spud Date(s):  3/13/2011
Completion Data
   Pool: BAKKEN     Perfs: 10889-20457     Comp: 9/18/2011     Status: F     Date: 9/20/2011     Spacing: 2SEC
   Pool: BAKKEN     Status: LOC     Date: 10/28/2015
Cumulative Production Data
   Pool: BAKKEN     Cum Oil: 36676     Cum MCF Gas: 50940     Cum Water: 23839
Production Test Data
   IP Test Date: 9/20/2011     Pool: BAKKEN     IP Oil: 1162     IP MCF: 393     IP Water: 451
Monthly production data since 8/15:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN2-20161000000
BAKKEN1-2016144020000
BAKKEN12-20151615931920612170717070
BAKKEN11-20152017681539432157415740
BAKKEN10-201593114672853563560
BAKKEN9-201520508480362509187322
BAKKEN8-201519574422540706463243
BAKKEN7-201522687951657880663217
BAKKEN6-201525576432645967538429

Monthly production data for prior year:

PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN8-201519574422540706463243
BAKKEN7-201522687951657880663217
BAKKEN6-201525576432645967538429
BAKKEN5-20153188496487615831130453
BAKKEN4-201520673564567740549191
BAKKEN3-20152687781485419151562353
BAKKEN2-2015281225147714261109986124
BAKKEN1-2015144184556824070407
BAKKEN12-20140000000
BAKKEN11-20144163002470247
BAKKEN10-2014122683552133703700
BAKKEN9-201430794782726672047

First six months production:

BAKKEN2-2012720700407152254
BAKKEN1-201224302830390495104951
BAKKEN12-201111314401900190
BAKKEN11-2011296197790000
BAKKEN10-20110000000
BAKKEN9-201113152012631220402204

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