Wednesday, December 16, 2015

Random Look At HRC Eagle Nest Well -- December 16, 2015 -- 10,000 Bbls Produced Over 4 Days

There are five wells on this pad, all running to the north:
  • 28280, see below;
  • 28281, conf, huge well, started producing 6/15;
  • 25502, 3,161, t6/15; cum 117K 10/15; produced 41K in the month of July, 2015
  • 24417, 2,174, t6/15; cum 74K 10/15;
  • 24418, 2,054, t6/15; cum 75K 10/15;
There are five wells to the east in the same section (a 3-well pad, and two singletons):
  • 30267, loc, one has to assume this one was not completed at same time as the others due to price environment
  • 30268, conf, huge well,
  • 30269, conf, huge well;
  • 18094, 1,323, t2/10; cum 246K 10/15 (was off-line 5/15 - 7/15)
  • 21066, 1,347, t1/12; cum 220K 10/15 (was off-line 6/15 - 8/15)
This well came off confidential list today:
  • 28280, 2,616, HRC, Fort Berthold 148-94-17C-8-6H, Eagle Nest, Sherman pad, 54 stages, 4.5 million lbs, t6/15; cum 86K 10/15; 
Side tracks:
  • 12/24/14: shale strike at 14,921 feet; tripped out and then side tracked started at 14,131 to 14,139 feet.
  • 12/25/14: attempt to side track failed; tripped out and began other side track at 13,760 to 13,789 feet.
  • 12/27/14: second side track attempt failed; tripped out and began another side track at 13,068 to 13,112 feet.
  • 12/31/14: successful third side track from 13,112 until experiencing another shale strike at 17,390 feet; tripped out and began a side track at 16,390 to 16,430 feet.
  • 12/20/15: after another side track fail at 15,652, operator tripped out and side tracked once more beginning at 15,712 feet and drilled to TD, 20,703 feet.
Production profile (note 10,409 bbls over four days in September, 2015):

PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN10-20152311968117968475100909574355
BAKKEN9-2015410409103727236968079551697
BAKKEN8-20151499241022294971079653885310
BAKKEN7-20153133475341293917951853051636
BAKKEN6-20151520342191522953526192026087

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