Sunday, September 20, 2015

Random Update On A CLR Holstein Well That Was Plugged Despite Great 30-Day IP -- September 20, 2015

Previous update:
February 17, 2015: this well was IA/SI (inactive/shut-in) the day it came off the confidential list; during the slump in oil prices:
  • 27563, 420, CLR, Holstein Federal 1-25H, Elm Tree, when I checked May 5, 2015, the frack data showed only one frack stage; the well was shown as active, having produced nicely in February and March, 2015, but no test date; was it fracked? Update: test date 2/11/15; cum 32K 5/15; only 10 days in 6/15;
Update, September 20, 2015: this looked like a very good well; it was surprising to see it be abandoned but now we have the explanation (see below):
  • 27563, PA/420, CLR, Holstein Federal 1-25H, Elm Tree, test date 2/11/15; cum 32K 5/15; only 10 days in 6/15;
The sundry form says the well was plugged and abandoned because a hole developed in the liner during stimulation operations. CLR says the plan is to come back to this well, "pull the remaining line or redrill a sidetrack."

PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN7-20150000000
BAKKEN6-20151073111181428400803
BAKKEN5-20153146984391116955674680639
BAKKEN4-20153075047767139778606687941
BAKKEN3-20153186839082165992128794178
BAKKEN2-201528100269169322310573952482

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