- 16772, 400, MRO, Pennington 41-4H, Reunion Bay, it appears the first frack was open hole, 386,420 pounds sand, t6/09; cum 195K 10/14;
This was the production profile the first few months after the well was completed and went on-line:
BAKKEN | 7-2009 | 27 | 5312 | 5166 | 1065 | 5339 | 0 | 5339 |
BAKKEN | 6-2009 | 27 | 6602 | 6878 | 2175 | 5613 | 0 | 5613 |
BAKKEN | 5-2009 | 2 | 577 | 0 | 517 | 490 | 0 | 490 |
This was the production profile in early 2012, about three years later:
BAKKEN | 6-2012 | 19 | 0 | 235 | 3 | 114 | 0 | 0 |
BAKKEN | 5-2012 | 3 | 222 | 0 | 38 | 163 | 82 | 78 |
BAKKEN | 4-2012 | 1 | 54 | 0 | 0 | 79 | 68 | 5 |
BAKKEN | 3-2012 | 20 | 1320 | 1528 | 222 | 1499 | 1154 | 235 |
BAKKEN | 2-2012 | 29 | 1980 | 1812 | 577 | 1804 | 1221 | 409 |
This was the production profile after the re-frack or whatever was done earlier this year (note, in July the well produced for only 12 days, producing 15,000 bbls):
BAKKEN | 7-2014 | 12 | 15072 | 15372 | 1409 | 2268 | 1621 | 422 |
BAKKEN | 6-2014 | 30 | 21773 | 21909 | 3624 | 4785 | 2827 | 1555 |
BAKKEN | 5-2014 | 13 | 20869 | 20384 | 2069 | 2361 | 0 | 2284 |
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