This is what makes the blog fun.
Sometime ago I noticed that a Stroh well reported 25 barrels/day on initial production, and suggested that there would be an explanation.
Shortly after that someone left a comment explaining a problem with the well. That was back in September (2010).
Today, I received a comment updating that well. The problem was fixed and they are ready to frack the well. That alone was very interesting. But the rest of the story: the unfracked well flowed at 960 barrels/day based on initial flowback. So, they will frack later this week.
For whole story, click here.
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