Updates
March 27, 2016: yes, the sundry form has finally been scanned in at the NDIC: 41 stages, 3.5 million lbs; other information below
November 4, 2015: yes, this well has been fracked. The information can be found at FracFocus; the lag time might be 3 - 4 weeks, but certainly not the lag time we see here. Fracking details:
- The frac job was from 6/2-6/6 2015
- ~110,000 bbls of fluid
- ~3.5 million lbs of proppant (All sand, no ceramics)
Original Post
- 30398, 1,891, Newfield, Gariety 150-98-30-31-4H, 15 days spud to TD, within the middle Bakken 100% of the time; 84.2% in the 15' primary middle Bakken target; 10.8% in the middle Bakken "B" facies; 5% in the middle Bakken "E" facies; Siverston, huge wall; t6/15; cum 282K 4/18;
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The NDIC scout ticket showing that this well is SI/NC:
NDIC File No: 30398
Well Type: OG Well Status: NC Status Date: 5/19/2015 Wellbore type: Horizontal Location: NWNW 5-150-98 Footages: 330 FNL 360 FWL Current Operator: NEWFIELD PRODUCTION COMPANY Current Well Name: GARIETY 150-98-6-7-4H Field: SIVERSTON Spud Date(s): 5/3/2015 Completion Data Pool: BAKKEN Status: SI Date: 5/19/2015 Cumulative Production Data Pool: BAKKEN Cum Oil: 98964 Cum MCF Gas: 172714 Cum Water: 38167 | |||||||||||||||||||||||||||||||||||||||||||||
Monthly Production Data
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