Tuesday, November 3, 2015

Certainly This Well Has Been Fracked -- November 3, 2015

Updates

March 27, 2016: yes, the sundry form has finally been scanned in at the NDIC: 41 stages, 3.5 million lbs; other information below

November 4, 2015: yes, this well has been fracked. The information can be found at FracFocus; the lag time might be 3 - 4 weeks, but certainly not the lag time we see here. Fracking details:
  • The frac job was from 6/2-6/6 2015
  • ~110,000 bbls of fluid
  • ~3.5 million lbs of proppant (All sand, no ceramics) 
Original Post
 
Certainly this well is fracked, but if not, natural fracking results in a great well. The well shows great production. The NDIC data shows that it is SI/NC. No fracking data at the file report.
  • 30398, 1,891, Newfield, Gariety 150-98-30-31-4H, 15 days spud to TD, within the middle Bakken 100% of the time; 84.2% in the 15' primary middle Bakken target; 10.8% in the middle Bakken "B" facies; 5% in the middle Bakken "E" facies;  Siverston, huge wall; t6/15; cum 282K 4/18;
 ********************************

The NDIC scout ticket showing that this well is SI/NC:

NDIC File No: 30398    
Well Type: OG     Well Status: NC     Status Date: 5/19/2015     Wellbore type: Horizontal
Location: NWNW 5-150-98     Footages: 330 FNL 360 FWL    
Current Operator: NEWFIELD PRODUCTION COMPANY
Current Well Name: GARIETY 150-98-6-7-4H
Field: SIVERSTON
Spud Date(s):  5/3/2015
Completion Data
   Pool: BAKKEN     Status: SI     Date: 5/19/2015
Cumulative Production Data
   Pool: BAKKEN     Cum Oil: 98964     Cum MCF Gas: 172714     Cum Water: 38167
Monthly Production Data
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN9-2015301799918107644434836323482218
BAKKEN8-2015312428124043686141091346966116
BAKKEN7-2015312771527487924148470395128680
BAKKEN6-201521289692875115621483171820029928
 

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