Tuesday, July 28, 2020

A Closer Look At The Well Coming Off Confidential List Today -- CLR Ogden - #36389 -- July 28, 2020

Highlights of the well that came off the confidential list today:
From the file report:
  • spud: August 6, 2019
  • cease drilling: August 14, 2019 (wow -- 8 days)
  • target: middle Bakken
  • TD: 20,263' MD
  • TVD: 10,172.33'
  • VS: 10,524.63'
  • drilled south to north; BH - NENE section 11-154-92
  • geological services began at 8,400' MD
  • KOP reached: 1:15 a.m. CDT, August 10, 2019
    • these are important dates and times, repeating, KOP reached 1:15 a.m. CST, August 10, 2019
  • drilling resumed at 9:00 a.m. CDT, same day, August 10, 2019 about eight hours later, to begin the curve
    • the last slide for the curve ended at 7:40 p.m. CST, August 10, 2019, so less than eleven hours to build the curve;
  • lateral: drilled out of the casing at 3:00 a.m. CDT, on August 12, 2019; 
    • gases ranged from100 - 1187 units, unremarkable;
  • the well reached TD of 20,263' MD at 12:45 a.m CST on August14, 2019; just under 48 hours;
    • the wellbore tracked throughout the middle Bakken formation for 100% of the lateral
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN5-202031156651560867502080520433342
BAKKEN4-202030190451911487542280022265506
BAKKEN3-2020312321523248805921127174403667
BAKKEN2-20202718248181061635715099015082

From FracFocus:
  • the well was fracked 11/24/2019 - 12/2/2019 -- 8 days; I generally see about ten days for a two-section lateral frack;
  • 8.158 million gallons of water; typical; moderate frack;
  • water by mass: 88.405%

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