Petro-Hunt Has A Monster Well In The Charlson WIth A Jump In Production In 11/18 -- October 26, 2019
For newbies:
- this well was drilled back in 2011 -- about 8 years ago
- as a Charlson well, it was a great well, but the typical Bakken decline took it to 3,000 bbls/month by 8/18, about a year ago
- in 10/18, after being off line for about a month, it showed a huge jump in production
- at 620,000 bbls cumulative, this is a monster well
The well:
- 19979, 817, Petro-Hunt, USA 153-95-22C-15-1H, Charlson, t7/11; cum 620K 8/19;
Recent production:
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
BAKKEN | 8-2019 | 29 | 6867 | 6776 | 3583 | 14906 | 8979 | 5746 |
BAKKEN | 7-2019 | 6 | 1565 | 1385 | 363 | 2394 | 1838 | 549 |
BAKKEN | 6-2019 | 6 | 1235 | 1405 | 591 | 2329 | 2287 | 0 |
BAKKEN | 5-2019 | 29 | 7640 | 7674 | 3177 | 15377 | 11459 | 3786 |
BAKKEN | 4-2019 | 30 | 8328 | 8374 | 3545 | 13546 | 13344 | 0 |
BAKKEN | 3-2019 | 31 | 9441 | 9621 | 4745 | 14730 | 14214 | 300 |
BAKKEN | 2-2019 | 28 | 6800 | 6617 | 3022 | 8548 | 8360 | 0 |
BAKKEN | 1-2019 | 31 | 11016 | 10996 | 4635 | 14465 | 14249 | 0 |
BAKKEN | 12-2018 | 31 | 12626 | 12616 | 5690 | 17252 | 15846 | 1190 |
BAKKEN | 11-2018 | 30 | 12152 | 12112 | 6023 | 17109 | 6170 | 10786 |
BAKKEN | 10-2018 | 20 | 10039 | 10029 | 5070 | 15201 | 13702 | 1499 |
BAKKEN | 9-2018 | 10 | 881 | 961 | 143 | 1750 | 1680 | 0 |
BAKKEN | 8-2018 | 31 | 2807 | 2756 | 540 | 5642 | 5371 | 55 |
BAKKEN | 7-2018 | 31 | 2820 | 2747 | 595 | 5331 | 4768 | 347 |
BAKKEN | 6-2018 | 30 | 2599 | 2584 | 712 | 5136 | 4435 | 492 |
BAKKEN | 5-2018 | 31 | 2791 | 2743 | 487 | 5607 | 5371 | 20 |
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