Saturday, October 26, 2019

Petro-Hunt Has A Monster Well In The Charlson WIth A Jump In Production In 11/18 -- October 26, 2019

For newbies:
  • this well was drilled back in 2011 -- about 8 years ago
  • as a Charlson well, it was a great well, but the typical Bakken decline took it to 3,000 bbls/month by 8/18, about a year ago
  • in 10/18, after being off line for about a month, it showed a huge jump in production
  • at 620,000 bbls cumulative, this is a monster well
The well:
  • 19979, 817, Petro-Hunt, USA 153-95-22C-15-1H, Charlson, t7/11; cum 620K 8/19;
Recent production:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN8-2019296867677635831490689795746
BAKKEN7-201961565138536323941838549
BAKKEN6-2019612351405591232922870
BAKKEN5-20192976407674317715377114593786
BAKKEN4-20193083288374354513546133440
BAKKEN3-2019319441962147451473014214300
BAKKEN2-201928680066173022854883600
BAKKEN1-2019311101610996463514465142490
BAKKEN12-2018311262612616569017252158461190
BAKKEN11-2018301215212112602317109617010786
BAKKEN10-2018201003910029507015201137021499
BAKKEN9-201810881961143175016800
BAKKEN8-201831280727565405642537155
BAKKEN7-2018312820274759553314768347
BAKKEN6-2018302599258471251364435492
BAKKEN5-201831279127434875607537120

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