APIs: 33-061-03984 and 33-061-03985. FracFocus is "down" right now (8:54 a.m. November 5, 2018).
First, let's look at #18884. Look at the production jump, note this well was drilled back in 2010:
- 18884, 625, EOG, Liberty 23-12H, Parshall, t9/10; cum 205K 9/18 --
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 9-2018 | 25 | 2001 | 2012 | 3353 | 1135 | 896 | 0 |
BAKKEN | 8-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 7-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 6-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 5-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 4-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 3-2018 | 10 | 125 | 130 | 206 | 99 | 15 | 10 |
BAKKEN | 2-2018 | 28 | 434 | 391 | 289 | 392 | 88 | 95 |
BAKKEN | 1-2018 | 31 | 599 | 611 | 217 | 816 | 449 | 141 |
BAKKEN | 12-2017 | 31 | 634 | 669 | 243 | 600 | 151 | 211 |
So, this well was taken off line six months ago, producing 500 bbls/month at that time; comes back on line and produces 2,000 bbls in 25 days. Analysts will suggest it was due to typical build in pressure while the well was off line.
What amazes me is how far away these three wells were -- that were taken off line when #33020 and #3020 were fracked. See this graphic:
#21406 was taken off line also. So at least four wells were taken off line while #33020 and #33021 were fracked.
No comments:
Post a Comment
Note: Only a member of this blog may post a comment.