Sunday, January 1, 2017

Nice Production After Being Returned To Status -- January 1, 2017

Production profile for:
  • 20629, 929, CLR, Patterson 1-13H, Camp, t10/11; cum 278K 1/17; although paperwork is sometimes delayed, the scout ticket shows this well as still flowing on its own; not on a pump;
Production profile for past couple of years:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN1-20173150675088328052724476338
BAKKEN12-201629666266293693734150381887
BAKKEN11-201628800677745605844461411873
BAKKEN10-20160000000
BAKKEN9-20160000000
BAKKEN8-20160000000
BAKKEN7-20160000000
BAKKEN6-20160000000
BAKKEN5-20161000770
BAKKEN4-201621895142272211038390
BAKKEN3-201631199120091565270222210
BAKKEN2-201629259324541837344219371055
BAKKEN1-201631284127911836404810302540
BAKKEN12-201518169714311750208118170
BAKKEN11-201574247021486300
BAKKEN10-2015283450366415188050371
BAKKEN9-2015142004132916813920180
BAKKEN8-20150000000
BAKKEN7-201584439144251161366674
BAKKEN6-201530189716921411411218101837
BAKKEN5-20153121102064163448593690690
BAKKEN4-20153022092339170542385073270
BAKKEN3-20153123802635184143992983620
BAKKEN2-20152822072306164739803763180
BAKKEN1-2015312937268624083832313320

Note increase in production from 2,000 bbls/oil/month back in 2015. It was taken of-line for a number of months while a neighboring well was being fracked.

When it came back on-line in 11/16, production jumped four-fold to over 8,000 bbls oil/ month.

No comments:

Post a Comment

Note: Only a member of this blog may post a comment.