Sunday, October 26, 2014

The Rosemary Eckelberg Is Back On Line; An EOG Wayzetta Well Also Back On-Line After Seven Months Of No Production -- October 26, 2014

Some housekeeping. Some months ago I noted that this well was taken off-line. I don't see an explanation in the well file. During the period that the well was taken off-line there were no new wells in the immediate area being drilled or fracked. Mostly likely a work-over back in the summer of 2013.

Regardless, it's back on-line.
  • 17310, Rosemary Eckelberg 41-26H, 459, 49,138 bbls in 15 months; went back on line 1/14; significant increase in oil production; no explanation in well file; t8/08; cum 127K 8/14;
A selected portion of the production history (sorry about the formatting, but one can probably figure it out):


PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN3-2014311398141122696036738
BAKKEN2-201428133414121739070739
BAKKEN1-20142511819422377960654
BAKKEN12-20130000000
BAKKEN11-20130000000
BAKKEN10-20130000000
BAKKEN9-20130000000
BAKKEN8-20130000000
BAKKEN7-2013161582352910439
BAKKEN6-20133056546113019358
BAKKEN5-2013317158271462353316
BAKKEN4-20133089991821536416132

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An EOG Wayzetta well is also back on line; this well went off-line in November, 2013, producing no oil until June, 2014; it is currently producing about 4,500 bbls of oil per month:
  • 16991, 1,383, EOG, Wayzetta 9-03H, Parshall field; short lateral, s4/08; producing 5,000 bbls 1/13; inactive since 5/13; back on status 7/13; no production since 11/13; back on status as of 6/14; t7/08; cum 785K 8/14;

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