Tuesday, July 10, 2018

Random Update Of An MRO Re-Fracked Chimney Butte Marlin Well - July 10, 2018

Updates

February 11, 2019: updated; full production profile here. first drilled in 2006; re-fracked in 2017 and the "new" well is better than the "old" well; this will be the Bakken going forward; we've discussed this often.


September 29, 2018: see update and other wells in this area. 

Original Post 

Look at the "small" re-frack. 

I would have thought I posted the production profile for this well, but I did not find it:
  • 16180, 128, MRO, Marlin 24-12H, Chimney Butte, t8/06; cum 319K 5/18; re-fracked 4/17 -- 14 stages, 2.8 million lbs (200,000 lbs/stage - standard)
Recent production profile:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN5-201815178017641117163214980
BAKKEN4-201810130413585446475000
BAKKEN3-2018314708471225663710315125
BAKKEN2-201828416041822536286123910
BAKKEN1-20183147314790503447703999220
BAKKEN12-201731473946424180597754010
BAKKEN11-201730731372883589460527281036
BAKKEN10-20173181548103464472835865501
BAKKEN9-201730768077497273745252131376
BAKKEN8-2017267497746410209533752880
BAKKEN7-2017289199919215776676867160
BAKKEN6-2017196679712011847607828632480
BAKKEN5-20177509645900468804113
BAKKEN4-20170000000
BAKKEN3-20170000000
BAKKEN2-201700320000
BAKKEN1-20174116460917412315
BAKKEN12-201631100610271301130837103
BAKKEN11-2016301102959130120599023
BAKKEN10-20163111589941391321103586

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