First, this well:
- 17940, 1,217, QEP/Questar, MHA 1-13-14H-150-91, McLean County, Deep Water Creek Bay field, t1/10; cum 356K 4/18; note this well was completed back in 2010; it showed the typical Bakken decline but then got a breath of fresh air in December, 2017. FracFocus shows that it was refracked in November, 2017. It was a small re-frack (and thus relatively inexpensive) -- only 6 million gallons of water and proppant constituting slightly less than 15% of total frack mix. The peak production (15,000 bbls in 1/18) was almost as much as the original frack.
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 4-2018 | 19 | 6816 | 6562 | 8853 | 2689 | 1733 | 248 |
BAKKEN | 3-2018 | 19 | 6690 | 6982 | 5953 | 3735 | 2202 | 670 |
BAKKEN | 2-2018 | 24 | 9105 | 8923 | 9480 | 4833 | 3508 | 390 |
BAKKEN | 1-2018 | 30 | 15035 | 15339 | 16952 | 8351 | 3834 | 3937 |
BAKKEN | 12-2017 | 31 | 19139 | 18697 | 37343 | 9084 | 3457 | 5219 |
BAKKEN | 11-2017 | 15 | 4519 | 4206 | 4180 | 1085 | 0 | 854 |
BAKKEN | 10-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 9-2017 | 6 | 241 | 252 | 169 | 1349 | 198 | 1151 |
BAKKEN | 8-2017 | 31 | 1436 | 1446 | 848 | 1054 | 1054 | 0 |
BAKKEN | 7-2017 | 31 | 1532 | 1588 | 918 | 1661 | 1238 | 2 |
BAKKEN | 6-2017 | 30 | 1659 | 1665 | 913 | 2095 | 792 | 895 |
BAKKEN | 5-2017 | 31 | 1792 | 1754 | 969 | 2099 | 321 | 1357 |
BAKKEN | 4-2017 | 30 | 1730 | 1746 | 970 | 1272 | 864 | 0 |
BAKKEN | 3-2017 | 22 | 1030 | 991 | 780 | 829 | 452 | 0 |
BAKKEN | 2-2017 | 22 | 946 | 960 | 581 | 702 | 349 | 0 |
Then, this well:
- 18172, 112, EOG, Fertile 35-23H, a Three Forks well; t9/09; cum 142K 4/18; this well was taken off-line back in November, 2016; prior to that it was a pretty lousy well; but then March, 2018, it was brought back on line. On January 29, 2018, the NDIC sent EOG a letter noting that this well had not produced in over a year, a violation of NDIC code. EOG was told to put this well back into production or submit request to plug and abandon. So it's back in production. Back in October, 2017, EOG requested this well be placed on IAW but apparently that was denied.
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 4-2018 | 30 | 620 | 645 | 1328 | 481 | 231 | 30 |
BAKKEN | 3-2018 | 14 | 590 | 537 | 1067 | 263 | 161 | 0 |
BAKKEN | 2-2018 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 1-2018 | 1 | 0 | 0 | 17 | 0 | 0 | 0 |
BAKKEN | 12-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 11-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 10-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 9-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 8-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 7-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 6-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 5-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 4-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 3-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 2-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 1-2017 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 12-2016 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 11-2016 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 10-2016 | 27 | 190 | 187 | 329 | 242 | 16 | 11 |
BAKKEN | 9-2016 | 30 | 302 | 306 | 484 | 291 | 47 | 0 |
BAKKEN | 8-2016 | 31 | 417 | 461 | 558 | 311 | 64 | 0 |
BAKKEN | 7-2016 | 31 | 450 | 390 | 595 | 335 | 80 | 3 |
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