Friday, January 20, 2017

The Helena Ruth Grant Wells

Reunion Bay, SWNW 33-150-93.
  • 30653, 1,755, WPX, Helena Ruth Grant 33-34HT, Three Forks, 41 stages, 6.1 million lbs; t12/16; cum 285K5/20; off line 5/20; remains off line 7/20; back on line; cum 326K 4/22;
  • 29081, 1,830, WPX, Helena Ruth Grant 33-34HW, Three Forks, 38 stages, 5.9 million lbs; t12/16; cum 321K 6/20; off line 7/20; back on line; cum 372K 4/22;
  • 29082, 2,397, WPX, Helena Ruth Grant 33-34HA, middle Bakken, 40 stages, 6.1 million lbs; t11/16; cum 364K 7/20; cum 416K 4/22;
  • 29083, 1,709, WPX, Helena Ruth Grant 33-34HX, Three Forks, t10/16; 41 stages, 6.1 million lbs; t10/16; cum 348K 7/20; cum 413K 4/22;
  • 29084, 1,900, WPX, Helena Ruth Grant 33-34HY, Three Forks, t10/16; 40 stages, 6 million lbs; t10/16; cum 296K 7/20; cum 350K 4/22;
  • 29085, 2,557, WPX, Helena Ruth Grant 33-34HC, middle Bakken, t11/16; 41 stages, 6.1 million lbs; t11/16; cum 402K 6/20; off line 7/20; back on line; cum 458K 4/22;
  • 19516, AB/TA/798, WPX, Helena Ruth Grant 33-34H, middle Bakken, re-frack 1/16; 934,620 lbs; the re-frac went badly; returned to production simply to show they had production for January; but there are no current plans to go back and fish the coiled tubing that was lost in the wellbore on the re-frack. It looks to me as if once the other wells start producing, they may abandon this well, although it has produced the entire past year, albeit dropping off significantly in the past few months. Original frack 3/11; 25 stages; 2.7 million lbs; cum 375K 10/18; inactive as of 3/17; actually had a day of production in 10/18; back on active status; four days active 5/19 but no production; remains inactive 7/20; now AB;

See the incredible Caribou wells in the same area.

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