Updates
February 11, 2017: this one has me very, very perplexed. Note the production profiles of these three wells -- the jump in production in late 2016, in the middle Bakken well, #25961. The file record does not shed any light. At the bottom of the post, one can see where the horizontals are located. I see no evidence of any new fracking, and these wells were taken off-line for such a short period of time.
- 25960, Three Forks: put on pump in September, 2014
- 25961, middle Bakken: no pump according to NDIC paperwork; paperwork could be delayed
- 25962, Three Forks: put on pump in May, 2015
25960, Three Forks: put on pump in September, 2014
Monthly Production Data
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 12-2016 | 29 | 1473 | 1516 | 174 | 1791 | 1666 | 31 |
BAKKEN | 11-2016 | 30 | 4581 | 4462 | 441 | 6229 | 6142 | 0 |
BAKKEN | 10-2016 | 7 | 526 | 515 | 138 | 1115 | 928 | 166 |
BAKKEN | 9-2016 | 0 | 0 | 8 | 0 | 0 | 0 | 0 |
BAKKEN | 8-2016 | 5 | 168 | 193 | 68 | 65 | 49 | 0 |
BAKKEN | 7-2016 | 27 | 1202 | 1208 | 23 | 1931 | 1852 | 0 |
BAKKEN | 6-2016 | 30 | 1493 | 1489 | 71 | 982 | 895 | 0 |
BAKKEN | 5-2016 | 31 | 1561 | 1543 | 1365 | 671 | 581 | 0 |
BAKKEN | 4-2016 | 30 | 753 | 739 | 5480 | 349 | 261 | 0 |
BAKKEN | 3-2016 | 1 | 93 | 92 | 12 | 4 | 0 | 1 |
BAKKEN | 2-2016 | 1 | 37 | 84 | 1 | 0 | 0 | 0 |
BAKKEN | 1-2016 | 21 | 2158 | 2149 | 1169 | 906 | 820 | 22 |
25961, middle Bakken: no pump according to NDIC paperwork; paperwork could be delayed;
[Update, January, 2018: just prior to the jump in production: a work-over rig on site, and a new pump put in; no evidence that is was re-fracked; no sundry form to suggest a re-frack and FracFocus does not show a re-frack.]
Monthly Production Data
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 12-2016 | 0 | 0 | 14 | 0 | 0 | 0 | 0 |
BAKKEN | 11-2016 | 30 | 500 | 774 | 551 | 412 | 325 | 0 |
BAKKEN | 10-2016 | 30 | 13862 | 13881 | 3096 | 17176 | 17085 | 0 |
BAKKEN | 9-2016 | 27 | 12439 | 12202 | 3271 | 15651 | 15567 | 0 |
BAKKEN | 8-2016 | 6 | 1535 | 1626 | 840 | 1910 | 1756 | 135 |
BAKKEN | 7-2016 | 28 | 5878 | 5840 | 1664 | 6185 | 6103 | 0 |
BAKKEN | 6-2016 | 25 | 4748 | 4746 | 1523 | 6154 | 6081 | 0 |
BAKKEN | 5-2016 | 31 | 5361 | 5405 | 2904 | 8837 | 8747 | 0 |
BAKKEN | 4-2016 | 26 | 7369 | 7380 | 4447 | 7211 | 7135 | 0 |
BAKKEN | 3-2016 | 31 | 7726 | 7737 | 4101 | 7378 | 7285 | 0 |
BAKKEN | 2-2016 | 29 | 8986 | 8969 | 3109 | 9431 | 9101 | 243 |
BAKKEN | 1-2016 | 31 | 7707 | 7685 | 2316 | 3095 | 2895 | 106 |
25962, Three Forks: put on pump in May, 2015
Monthly Production Data
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 12-2016 | 21 | 3628 | 3502 | 2085 | 1522 | 1454 | 0 |
BAKKEN | 11-2016 | 30 | 3118 | 3036 | 2465 | 3478 | 3391 | 0 |
BAKKEN | 10-2016 | 10 | 294 | 288 | 1315 | 563 | 269 | 264 |
BAKKEN | 9-2016 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 8-2016 | 1 | 0 | 34 | 0 | 8 | 7 | 0 |
BAKKEN | 7-2016 | 26 | 1228 | 1258 | 1043 | 5780 | 5704 | 0 |
BAKKEN | 6-2016 | 30 | 2488 | 2502 | 2056 | 5446 | 5066 | 293 |
BAKKEN | 5-2016 | 28 | 3486 | 3498 | 3224 | 7586 | 7504 | 0 |
BAKKEN | 4-2016 | 30 | 4061 | 4062 | 8999 | 7978 | 7891 | 0 |
BAKKEN | 3-2016 | 31 | 4002 | 3970 | 2883 | 6869 | 6777 | 0 |
BAKKEN | 2-2016 | 29 | 2871 | 2826 | 3259 | 4639 | 4552 | 0 |
BAKKEN | 1-2016 | 7 | 624 | 629 | 755 | 701 | 680 | 0 |
****************************************
February 8, 2017: frack data from FracFocus
- 26419, BR: 33-053-05259, 1/23/14 - 1/25/14; 2.1 million gallons water; 82% water by mass; 16% sand by mass;
- 17356, BR: 33-053-02902, no data at FracFocus,
- 26007, BR, API: 33-053-05133, 1/18/14 - 1/21/14; 2.4 million gallons water; 84% water by mass; 15% sand by mass;
- 26006, BR, API: 33-053-05132, 1/15/14 - 1/18/14; 2.3 million gallons water; 83% water by mass; 15% sand by mass;
Original Post
Comment regarding "the post" below.
I think the data in "the post" below and what it might be showing is quite staggering. (I haven't pointed out everything but the data is there.)
Take a look at the data.
For those of you with a "basic subscription" there is even more to this story which I will post at a later date, but tonight I'm too tired. In addition, I need to reflect on this one for awhile. It's possible I made a mistake; too much data; need to confirm later.
Disclaimer: in a long note like this there will be typographical and factual errors. I am doing this for my benefit only. I am probably seeing things that don't exist. Don't quote me on any of this. Again, this is for my interest and benefit only. I post it with the rest of the blog, because I don't want the aggravation of two blogs, one private, one public. Feel free to read it but again, don't quote me on it. It's probably just "one of those things." If this is important to you, go to the source.
The Post
- in the autumn of 2013, this well was producing around 1,500 bbls of oil / month
- then, knowing that by simply taking a well off-line for a "significant" period of time (for purpose of discussion, 3 - 7 months) could significantly increase production, BR apparently took this well off-line for a few months beginning in November, 2013
- BR brought the well back on line in March, 2014, and within a month or so, production jumped to over 26,000 bbls of oil per month
- that "26,000 bbls" was just "oil"; natural gas also showed a similar jump; produced water also jumped, but in the big scheme of things, and compared to a lot of Bakken wells, the amount of produced water was trivial
It's possible the oil was commingled in a battery of tanks and there was an error in the data regarding how much oil this well produced. There are all kinds of things that might provide an alternate explanation. If commingling was an error, to the best of my knowledge natural gas produced, sold, and flared is not similarly affected but I could be wrong.
Production profile since initial production to the present (still active):
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 12-2016 | 17 | 2102 | 2092 | 123 | 1998 | 1956 | 0 |
BAKKEN | 11-2016 | 29 | 3616 | 3397 | 1057 | 4950 | 4878 | 0 |
BAKKEN | 10-2016 | 17 | 1762 | 2029 | 906 | 2144 | 1262 | 840 |
BAKKEN | 9-2016 | 23 | 3023 | 2810 | 434 | 5122 | 5012 | 53 |
BAKKEN | 8-2016 | 31 | 3931 | 3874 | 1878 | 5870 | 1439 | 4354 |
BAKKEN | 7-2016 | 31 | 3951 | 3608 | 1293 | 5189 | 3871 | 1241 |
BAKKEN | 6-2016 | 11 | 1326 | 1867 | 390 | 2342 | 2051 | 263 |
BAKKEN | 5-2016 | 10 | 839 | 549 | 599 | 1578 | 1212 | 341 |
BAKKEN | 4-2016 | 30 | 3584 | 3591 | 335 | 8002 | 7559 | 368 |
BAKKEN | 3-2016 | 31 | 3378 | 3590 | 409 | 7486 | 7039 | 370 |
BAKKEN | 2-2016 | 27 | 3258 | 3294 | 342 | 6434 | 5950 | 417 |
BAKKEN | 1-2016 | 31 | 3558 | 3311 | 362 | 7062 | 6784 | 202 |
BAKKEN | 12-2015 | 31 | 3715 | 3645 | 473 | 6689 | 4546 | 2066 |
BAKKEN | 11-2015 | 30 | 3828 | 4129 | 424 | 5709 | 5327 | 307 |
BAKKEN | 10-2015 | 31 | 4260 | 4038 | 353 | 7805 | 7728 | 0 |
BAKKEN | 9-2015 | 19 | 3048 | 3122 | 324 | 4182 | 2995 | 1139 |
BAKKEN | 8-2015 | 22 | 3169 | 3472 | 271 | 4837 | 2057 | 2725 |
BAKKEN | 7-2015 | 30 | 4469 | 4059 | 399 | 6882 | 5381 | 1427 |
BAKKEN | 6-2015 | 30 | 4229 | 4218 | 399 | 6447 | 1174 | 5199 |
BAKKEN | 5-2015 | 31 | 4848 | 4780 | 354 | 7221 | 306 | 6838 |
BAKKEN | 4-2015 | 30 | 4512 | 4524 | 436 | 7100 | 512 | 6514 |
BAKKEN | 3-2015 | 31 | 4664 | 4610 | 551 | 3045 | 1831 | 1136 |
BAKKEN | 2-2015 | 26 | 4749 | 4783 | 226 | 7480 | 0 | 7416 |
BAKKEN | 1-2015 | 30 | 6774 | 7099 | 683 | 10670 | 0 | 10595 |
BAKKEN | 12-2014 | 9 | 1371 | 964 | 246 | 1632 | 0 | 1609 |
BAKKEN | 11-2014 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 10-2014 | 15 | 3079 | 3543 | 228 | 3646 | 0 | 3609 |
BAKKEN | 9-2014 | 26 | 9109 | 8968 | 1134 | 9867 | 0 | 9802 |
BAKKEN | 8-2014 | 29 | 16093 | 15960 | 1794 | 17778 | 0 | 17706 |
BAKKEN | 7-2014 | 31 | 22414 | 22795 | 2875 | 24206 | 53 | 24075 |
BAKKEN | 6-2014 | 30 | 26910 | 26451 | 2820 | 9604 | 96 | 9434 |
BAKKEN | 5-2014 | 31 | 24397 | 24866 | 3068 | 864 | 46 | 741 |
BAKKEN | 4-2014 | 25 | 20922 | 20448 | 2441 | 1345 | 0 | 1283 |
BAKKEN | 3-2014 | 12 | 8905 | 8789 | 1096 | 6005 | 2746 | 3230 |
BAKKEN | 2-2014 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 1-2014 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 12-2013 | 1 | 0 | 0 | 0 | 3 | 0 | 0 |
BAKKEN | 11-2013 | 17 | 1167 | 1409 | 9 | 1275 | 1210 | 23 |
BAKKEN | 10-2013 | 31 | 1537 | 1626 | 67 | 2220 | 1781 | 361 |
BAKKEN | 9-2013 | 30 | 1463 | 1409 | 55 | 2257 | 1696 | 487 |
BAKKEN | 8-2013 | 31 | 1541 | 1633 | 62 | 2368 | 2174 | 118 |
BAKKEN | 7-2013 | 28 | 1550 | 1620 | 70 | 2295 | 2166 | 59 |
BAKKEN | 6-2013 | 30 | 1550 | 1373 | 78 | 2360 | 2254 | 32 |
BAKKEN | 5-2013 | 31 | 1809 | 1850 | 51 | 2619 | 2281 | 260 |
BAKKEN | 4-2013 | 20 | 1144 | 1137 | 35 | 1299 | 559 | 690 |
BAKKEN | 3-2013 | 31 | 1637 | 1443 | 48 | 2159 | 1650 | 432 |
BAKKEN | 2-2013 | 28 | 1534 | 1683 | 47 | 2230 | 2028 | 132 |
BAKKEN | 1-2013 | 31 | 1709 | 1554 | 51 | 2478 | 2180 | 221 |
BAKKEN | 12-2012 | 31 | 1683 | 1564 | 44 | 2409 | 2163 | 170 |
BAKKEN | 11-2012 | 30 | 1641 | 1950 | 42 | 2471 | 2219 | 178 |
BAKKEN | 10-2012 | 31 | 1709 | 1711 | 67 | 2565 | 2231 | 256 |
BAKKEN | 9-2012 | 30 | 1663 | 1608 | 72 | 2728 | 2328 | 325 |
BAKKEN | 8-2012 | 31 | 1707 | 1588 | 71 | 2579 | 2039 | 463 |
BAKKEN | 7-2012 | 31 | 1708 | 1851 | 70 | 2654 | 2056 | 521 |
BAKKEN | 6-2012 | 29 | 1727 | 1558 | 81 | 2878 | 2462 | 344 |
BAKKEN | 5-2012 | 27 | 1477 | 1726 | 80 | 2878 | 2307 | 504 |
BAKKEN | 4-2012 | 5 | 2026 | 1796 | 78 | 2773 | 0 | 2761 |
BAKKEN | 3-2012 | 4 | 1899 | 1917 | 140 | 2927 | 0 | 2917 |
BAKKEN | 2-2012 | 4 | 1847 | 1714 | 67 | 2867 | 0 | 2857 |
BAKKEN | 1-2012 | 4 | 1747 | 1938 | 50 | 7257 | 4536 | 2711 |
BAKKEN | 12-2011 | 5 | 1982 | 1912 | 73 | 2960 | 0 | 2947 |
BAKKEN | 11-2011 | 3 | 1954 | 2088 | 66 | 2932 | 0 | 2924 |
BAKKEN | 10-2011 | 10 | 1952 | 1868 | 68 | 3278 | 321 | 2932 |
BAKKEN | 9-2011 | 6 | 1972 | 2076 | 94 | 3867 | 811 | 3056 |
BAKKEN | 8-2011 | 4 | 2117 | 1879 | 81 | 3276 | 0 | 3276 |
BAKKEN | 7-2011 | 24 | 2087 | 2300 | 97 | 3143 | 270 | 2873 |
BAKKEN | 6-2011 | 28 | 1950 | 2007 | 144 | 2682 | 133 | 2549 |
BAKKEN | 5-2011 | 31 | 2277 | 2365 | 82 | 3195 | 512 | 2684 |
BAKKEN | 4-2011 | 30 | 2458 | 2356 | 112 | 3826 | 882 | 2944 |
BAKKEN | 3-2011 | 31 | 3008 | 2918 | 128 | 4432 | 464 | 3969 |
BAKKEN | 2-2011 | 9 | 1583 | 1645 | 28 | 2917 | 888 | 2029 |
BAKKEN | 1-2011 | 3 | 637 | 701 | 0 | 2594 | 1732 | 862 |
BAKKEN | 12-2010 | 24 | 1920 | 1934 | 74 | 2586 | 2336 | 250 |
BAKKEN | 11-2010 | 30 | 2350 | 2075 | 99 | 3181 | 2429 | 752 |
BAKKEN | 10-2010 | 31 | 2397 | 2561 | 129 | 3126 | 755 | 2372 |
BAKKEN | 9-2010 | 29 | 2416 | 2534 | 134 | 3398 | 1860 | 1538 |
BAKKEN | 8-2010 | 31 | 2634 | 2766 | 169 | 3697 | 0 | 3697 |
BAKKEN | 7-2010 | 31 | 2575 | 2285 | 287 | 3541 | 69 | 3472 |
BAKKEN | 6-2010 | 22 | 1286 | 1294 | 482 | 1570 | 246 | 1324 |
BAKKEN | 5-2010 | 9 | 1146 | 952 | 403 | 1349 | 198 | 1151 |
BAKKEN | 4-2010 | 6 | 1404 | 1363 | 51 | 1016 | 1016 | 0 |
BAKKEN | 3-2010 | 28 | 2795 | 3104 | 104 | 4719 | 3166 | 1553 |
BAKKEN | 2-2010 | 28 | 2804 | 2616 | 96 | 5502 | 3909 | 1593 |
BAKKEN | 1-2010 | 31 | 3723 | 4075 | 136 | 5190 | 2894 | 2296 |
BAKKEN | 12-2009 | 6 | 2696 | 2285 | 103 | 2541 | 421 | 2120 |
BAKKEN | 11-2009 | 28 | 3482 | 3616 | 281 | 5207 | 1571 | 3636 |
BAKKEN | 10-2009 | 19 | 2782 | 2744 | 494 | 3789 | 687 | 3102 |
BAKKEN | 9-2009 | 24 | 2846 | 2953 | 87 | 3853 | 0 | 3853 |
BAKKEN | 8-2009 | 22 | 3716 | 3630 | 130 | 5111 | 0 | 5111 |
BAKKEN | 7-2009 | 31 | 4709 | 4674 | 211 | 1690 | 0 | 1690 |
BAKKEN | 6-2009 | 28 | 4244 | 4237 | 226 | 4388 | 18 | 4370 |
BAKKEN | 5-2009 | 31 | 4448 | 4407 | 125 | 4088 | 1312 | 2776 |
BAKKEN | 4-2009 | 30 | 4460 | 4476 | 734 | 5078 | 1082 | 3996 |
BAKKEN | 3-2009 | 5 | 304 | 422 | 417 | 223 | 9 | 214 |
BAKKEN | 2-2009 | 17 | 3781 | 3672 | 132 | 4700 | 3661 | 1039 |
BAKKEN | 1-2009 | 26 | 5551 | 5994 | 200 | 7999 | 6356 | 1643 |
BAKKEN | 12-2008 | 29 | 7042 | 6609 | 298 | 8622 | 429 | 8193 |
BAKKEN | 11-2008 | 30 | 7526 | 7272 | 2071 | 4908 | 4908 | 0 |
This is what the production profile looked like during those twelve months:
BAKKEN | 10-2014 | 15 | 3079 | 3543 | 228 | 3646 | 0 | 3609 |
BAKKEN | 9-2014 | 26 | 9109 | 8968 | 1134 | 9867 | 0 | 9802 |
BAKKEN | 8-2014 | 29 | 16093 | 15960 | 1794 | 17778 | 0 | 17706 |
BAKKEN | 7-2014 | 31 | 22414 | 22795 | 2875 | 24206 | 53 | 24075 |
BAKKEN | 6-2014 | 30 | 26910 | 26451 | 2820 | 9604 | 96 | 9434 |
BAKKEN | 5-2014 | 31 | 24397 | 24866 | 3068 | 864 | 46 | 741 |
BAKKEN | 4-2014 | 25 | 20922 | 20448 | 2441 | 1345 | 0 | 1283 |
BAKKEN | 3-2014 | 12 | 8905 | 8789 | 1096 | 6005 | 2746 | 3230 |
BAKKEN | 2-2014 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 1-2014 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 12-2013 | 1 | 0 | 0 | 0 | 3 | 0 | 0 |
BAKKEN | 11-2013 | 17 | 1167 | 1409 | 9 | 1275 | 1210 | 23 |
BAKKEN | 10-2013 | 31 | 1537 | 1626 | 67 | 2220 | 1781 | 361 |
BAKKEN | 9-2013 | 30 | 1463 | 1409 | 55 | 2257 | 1696 | 487 |
BAKKEN | 8-2013 | 31 | 1541 | 1633 | 62 | 2368 | 2174 | 118 |
BAKKEN | 7-2013 | 28 | 1550 | 1620 | 70 | 2295 | 2166 | 59 |
BAKKEN | 6-2013 | 30 | 1550 | 1373 | 78 | 2360 | 2254 | 32 |
BAKKEN | 5-2013 | 31 | 1809 | 1850 | 51 | 2619 | 2281 | 260 |
BAKKEN | 4-2013 | 20 | 1144 | 1137 | 35 | 1299 | 559 | 690 |
Another interesting thing about this well: look at the initial production. The best this well did after a "deliberate frack" was about 7,526 bbls of oil. By simply shutting this well in for a few months in late 2013, and bringing it back on-line, production jumped more than 3-fold, for several months:
BAKKEN | 6-2009 | 28 | 4244 | 4237 | 226 | 4388 | 18 | 4370 |
BAKKEN | 5-2009 | 31 | 4448 | 4407 | 125 | 4088 | 1312 | 2776 |
BAKKEN | 4-2009 | 30 | 4460 | 4476 | 734 | 5078 | 1082 | 3996 |
BAKKEN | 3-2009 | 5 | 304 | 422 | 417 | 223 | 9 | 214 |
BAKKEN | 2-2009 | 17 | 3781 | 3672 | 132 | 4700 | 3661 | 1039 |
BAKKEN | 1-2009 | 26 | 5551 | 5994 | 200 | 7999 | 6356 | 1643 |
BAKKEN | 12-2008 | 29 | 7042 | 6609 | 298 | 8622 | 429 | 8193 |
BAKKEN | 11-2008 | 30 | 7526 | 7272 | 2071 | 4908 | 4908 | 0 |
Initial production was not particularly remarkable. This was an open-hole/perforated frack in October/November, 2008. It was tested November 12, 2008. Frack: 647,200 lbs of white sand; 9,103 bbls of water gel; sliding sleeves.
Based on the file report, this was the only frack. I did not see any reports of any work-over rig action. FracFocus did not have any frack data.
Back-of-the-envelope:
- this jump in production was back in early 2014
- let's say oil at the well head was $75/bbl
- let's say a mineral owner had a 3/8th interest
- 1,500 bbls/month = $42,000 (one month)
- 26,000 bbls/month = $731,250 (one month)
- 17356, 356, BR, Archer 14-25H, Charlson, t11/12/08; cum 366K 12/16
This ain't no party,
This ain't no disco,
This ain't no fooling around
No time for dancing,
I ain't got time for that now
Heard about Houston?
Heard about Detroit?
Heard about Pittsburgh, PA?
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