- 35065, 520, was SI/NC-->conf, Enerplus Map 152-94-33D-28H-TF1, Antelope, t9/19; cum 141K 1/20; F; 43 stages; 15.6 million lbs; (there is a common map turtle),
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
SANISH | 1-2020 | 30 | 38138 | 38106 | 16036 | 60907 | 51167 | 9629 |
SANISH | 12-2019 | 31 | 42033 | 41969 | 23828 | 67126 | 39114 | 27916 |
SANISH | 11-2019 | 27 | 32033 | 31772 | 19060 | 51157 | 38171 | 12618 |
SANISH | 10-2019 | 16 | 14284 | 14391 | 21489 | 22813 | 10691 | 12086 |
SANISH | 9-2019 | 13 | 14606 | 14409 | 28127 | 29212 | 5109 | 24077 |
From the file report:
- spud: January 12, 2019
- TD: May 10, 2019;
- total days: 18
- total drilling days: 178.2
- True Rig 40
- vertical section: 9,833.9 at TD;
- KOP: 10,173' TVD;
- lateral footage: 10,096';
- it looks like it took about 1.5 days to drill the curve; it took two extra trips during the curve due to lack of build rates;
- slightly less than full four days to drill the lateral; no trips occurred in the lateral portion;
- background gas ranged from 500 - 1600 units; connection gases ranged from 800 - 2400 units;
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