Previous update:
February 17, 2015: this well was IA/SI (inactive/shut-in) the day it came off the confidential list; during the slump in oil prices:
- 27563, 420, CLR, Holstein
Federal 1-25H, Elm Tree, when I checked May 5, 2015, the frack data
showed only one frack stage; the well was shown as active, having
produced nicely in February and March, 2015, but no test date; was it
fracked? Update: test date 2/11/15; cum 32K 5/15; only 10 days in 6/15;
Update, September 20, 2015: this looked like a very good well; it was surprising to see it be abandoned but now we have the explanation (see below):
- 27563, PA/420, CLR, Holstein
Federal 1-25H, Elm Tree, test date 2/11/15; cum 32K 5/15; only 10 days in 6/15;
The sundry form says the well was plugged and abandoned because a hole developed in the liner during stimulation operations. CLR says the plan is to come back to this well, "pull the remaining line or redrill a sidetrack."
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
BAKKEN | 7-2015 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 6-2015 | 10 | 731 | 1118 | 142 | 840 | 0 | 803 |
BAKKEN | 5-2015 | 31 | 4698 | 4391 | 1169 | 5567 | 4680 | 639 |
BAKKEN | 4-2015 | 30 | 7504 | 7767 | 1397 | 7860 | 6687 | 941 |
BAKKEN | 3-2015 | 31 | 8683 | 9082 | 1659 | 9212 | 8794 | 178 |
BAKKEN | 2-2015 | 28 | 10026 | 9169 | 3223 | 10573 | 9524 | 82 |
No comments:
Post a Comment
Note: Only a member of this blog may post a comment.