Saturday, October 19, 2019

Random Look At A Mediocre MRO Well That Became A Huge Well -- October 19, 2019

Note: this well was drilled back in 2009; it had a very, very small initial production (see second spreadsheet below. Then five years later, in 2014, this very, very mediocre well had a huge jump in production and overnight went from a mediocre well to a great well.

The well:
  • 17771, 585, MRO, Jay Sandstrom USA 34-31H, 33-061-00909, Reunion Bay, t3/09; cum 542K 10/20; off line 11/20; fracked 6/26/14 - 6/28/14; 1.7 million gallons of water; 85.4% water by mass; original frack, 2/21/09, open hole; 0 stages; second frack, 6/26/14, 30 stages; 1.8 million lbs proppant;
Period of interest:

BAKKEN4-201523716172412330797852351844
BAKKEN3-2015309506954330851208395231375
BAKKEN2-201528107151063536581174591401291
BAKKEN1-20153113103131454340114077009120
BAKKEN12-2014311579515865533013411117310364
BAKKEN11-201430184761883964811611899112974
BAKKEN10-2014312708627028103522319623519851
BAKKEN9-201426174711742189301379079243872
BAKKEN8-20143121192208961023317698105774667
BAKKEN7-2014131277212746571090309460
BAKKEN6-20141142021190104
BAKKEN5-20140000000
BAKKEN4-20141189014591428250665
BAKKEN3-2014312724221147530301867696
BAKKEN2-2014281949203039522261729113
BAKKEN1-201431162914242231325772223
BAKKEN12-2013144664762711711773
BAKKEN11-201319111411211691348934301
BAKKEN10-2013311876217625620741755133

Drilled back in 2009, this was the initial production for this well:
BAKKEN8-20093146504712615445504455
BAKKEN7-20093154195681722518705187
BAKKEN6-20092844694446753429704297
BAKKEN5-20093150304860698479304793
BAKKEN4-20092957615662877551605516
BAKKEN3-200931935592232285843908439
BAKKEN2-20095297525371627252902529

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