The well:
- 24224, 681, CLR, Hawkinson 5-22H, 33-025-01954; Oakdale, middle Bakken, 30 stages, 2.8 million lbs, t9/13; cum 411K 41/9; went offline 3/19; not recently fracked;
Pool | Date | Days | BBLS Oil | Runs | BBLS Water | MCF Prod | MCF Sold | Vent/Flare |
---|---|---|---|---|---|---|---|---|
BAKKEN | 9-2019 | 21 | 10631 | 10436 | 9188 | 12918 | 8580 | 2110 |
BAKKEN | 8-2019 | 31 | 16031 | 16077 | 10425 | 24150 | 18984 | 3281 |
BAKKEN | 7-2019 | 30 | 19542 | 19385 | 12628 | 24345 | 19757 | 3044 |
BAKKEN | 6-2019 | 25 | 15682 | 15413 | 12784 | 18451 | 11897 | 5362 |
BAKKEN | 5-2019 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
BAKKEN | 4-2019 | 0 | 0 | 51 | 0 | 0 | 0 | 0 |
BAKKEN | 3-2019 | 19 | 1033 | 1092 | 414 | 3281 | 2942 | 74 |
BAKKEN | 2-2019 | 28 | 1482 | 1511 | 303 | 5279 | 4591 | 113 |
BAKKEN | 1-2019 | 31 | 1226 | 1336 | 781 | 4008 | 3444 | 18 |
BAKKEN | 12-2018 | 31 | 1837 | 1766 | 740 | 9138 | 7633 | 282 |
BAKKEN | 11-2018 | 30 | 1885 | 1800 | 849 | 8441 | 7254 | 284 |
BAKKEN | 10-2018 | 31 | 1556 | 1560 | 602 | 9797 | 8986 | 67 |
BAKKEN | 9-2018 | 30 | 2196 | 2223 | 339 | 11221 | 10638 | 9 |
So, what's the deal. It took a bit of sleuthing, but here's the answer. The sister wells on this pad, #24223 and #24225 also showed a significant jump in production.
It was obvious a neighboring well (or wells) had been recently fracked. None of the other Hawkinson wells had been recently fracked, and none of the others to the east showed a jump in production.
However, there it was, right on cue, a CLR Carus well in the neighboring drilling unit to the west had been fracked in 4/19. So, halo phenomenon. Clear as drilling mud.
The Saudis have not commented on this phenomenon but it is real and does effect the EUR.
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