Saturday, October 22, 2016

Better Late Than Never -- It's Not Done Until The Paperwork Is Done -- October 22, 2016

Update on this well that I noted went off-line back in November, 2015:

  • 18575, 1,007/IA, Slawson, Hunter 1-8-17H, Big Bend, t6/11; cum 453K 8/16; off-line all of 11/15; only one day production 1/16; only one day production 2/16; IA as of 3/16; back on line as of 6/16;
This is a screenshot of the 6-well pad. Four "Hunter" wells run south; two Jeriyote wells run north. Four of the six wells all went off-line for the same period of time, back in early 2016.



Production profile for #18575 since June, 2015:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN8-20163174787652134759485689104
BAKKEN7-20163170076967212856645199310
BAKKEN6-20163076437861186462755563562
BAKKEN5-20164109038433383675264
BAKKEN4-201616100500
BAKKEN3-20160000000
BAKKEN2-20161000610
BAKKEN1-2016117133814315511634
BAKKEN12-201528322930152841260724670
BAKKEN11-201500390000
BAKKEN10-201530458347762086364623521144
BAKKEN9-20153070056671242954234697576
BAKKEN8-201531492051074615400822371616
BAKKEN7-20153168086929427052374677405
BAKKEN6-201530458845684657375823641244

The production profile back in 2012. Note the production jump in February, 2012:
Bakken 10-2012319810101522502720468940
BAKKEN9-2012301102910809276810981106810
BAKKEN8-2012301583015806374013944136440
BAKKEN7-201231777377032306543151210
BAKKEN6-201227710066712022474544750
BAKKEN5-2012311435015035336110501101910
BAKKEN4-20123012645122003412819378930
BAKKEN3-20123111427120394021733570250
BAKKEN2-20122914320140873735819479040
BAKKEN1-201223713470621250352732970
BAKKEN12-201120566456511434342532250

Better late than never.

A sundry report was received by the NDIC on April 4, 2016. The sundry form was dated March 30, 2016. However, the sundry form says the "workover" was started on/about February 2, 2012, and completed February 3, 2012. 

If the "work done" dates are correct, it took about four years for this sundry form to get to the NDIC. 

If the workover was accomplished in February, 2016, then the NDIC dates make sense, and the work would coincide with the well being taken off-line in February, 2016.

But based on the scout report, I think this was simply a pump being put in place as of 2/3/2012. But the production profile shows that there were no down days in February, 2012. 

The "details of work" have too many acronyms for me to sort out everything. If anyone is interested in parsing this one, go for it:
POOH, w/ tbg, & Pkr, W/ Ceramic Disk. LD same. MU & RIH w/ 2 jts, 2 7/8" L-80 tbg. Bll Plugged, 3 1/2" OD Slawson Gas Sep, 1 Jt, 2 7/8" tbg, WeatherfordTHBM 3 1/2" x 2 3/4" x 24' x 30' Tbg. Barrel Pump, w/SN, 1 Jt, 3 1/2" L-80 tbg, 7" Weatherford TAC, 6Jts, 2 7/8" L-80 Duraseal L-80 tbg, & 287 Jts, 2 7/8" L-80 prod, tbg, ND BOP, Set TAC in 21K Tension w/42" Stretch. NU B-1 Flange, NU Rattagin, Pumping Tee w/ Valves. RD Tbg. Equip, RU for rods. Spot in Rod trailer, Prep K-Bars & entire rod string w/ cplgs. RU Floor for PU Rods. PU ON/Off Tool on slick 1 1/2" K-Bar for engaging on Plunger, PU 1 more 1 1/2" Slick K-Bar, PU 8 - 1 1/2" K-Bar w/ 1" x 36" Centr.

PU & RIH w/ 100 - 3/4" New Norris Plain 78's. 125 - 7/8" New Norris Plain 78's, & 139 - 1" New Norris 78's Plain rods.

Get Tag, Mark rod, & LD 2 - 1" rods. Measure & PU 1" x 4' & 1" x 2' Ponys, Prep & dress 1 1/2" x 30' Metal Spray Polish Rod. Engage over Plunder, & long stroke Pump.

OKFill tbg, w/ 3 BSW & Test to 600 Psi. OK, stroke well up w/ rig to 500 Psi, OK. Put Mark II Unit together, PU head on Lufkin Rep, set & program Panel w/ down howl info. Start Unit & ck. for Tag & alignment. OK. Clean up entire location.

Watch well for 30 Min. Pumping good & smooth. SDFD.
Or, "Pump assembled, in place. Stroke tested okay. Site cleaned up. Shut down for day (SDFD). 

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