Wednesday, August 23, 2017

Random Update Of An MRO Re-Fracked Well -- August 23, 2017

The well:
  • 16753, 314, MRO, Repp 34-34H, Bailey, t1/08; cum 153K 6/17, recent production:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN6-20171814004139251008470368194617
BAKKEN5-201712709214011
BAKKEN4-20172645139712438559127
BAKKEN3-20173156659715946017541
BAKKEN2-2017285216111444362075
BAKKEN1-2017315825481584982455
BAKKEN12-2016315395421584632145
BAKKEN11-20163060958215445319315
BAKKEN10-2016316005871584642131
BAKKEN9-20163058857814540910264
BAKKEN8-20163158356218338212122
BAKKEN7-2016315896321663784125
BAKKEN6-2016305775731613816133
BAKKEN5-2016316016231693888130

Re-fracked: 5/25/2017; 45 stages; 5.6 million lbs; from the file report: "Originally an open hole completion in 2008. MRO cleaned out lateral and did 45-stage cemented liner plug and perf style completion."

Production when first fracked:
BAKKEN7-2008193132271515748378370
BAKKEN6-200822202523186427207200
BAKKEN5-20083129792916802103810380
BAKKEN4-20083027562930674109110910
BAKKEN3-200831414638941242137513750
BAKKEN2-200829542152501627598350248
BAKKEN1-200814421341151882000

Two neighboring wells:
  • to the west, 18842, taken off-line 5/17; still waiting to see what production will be when brought back on status;
  • to the east, 18736, never taken off-line; no bump in production noted, but need to check back in a few months;

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