Thursday, March 16, 2017

Random Update On One Of The Whiting Flatland Federal Wells In Twin Valley -- March 16, 2017

Updates

June 16, 2017; FracFocus does not show any re-frack for this well. This post explains why #30774 might have been taken off-line for a couple of months in 2016.
 
Original Post
 
To the best of my knowledge, this well was fracked only once. FracFocus has data for only one frack: September 17 - 23, 2015. This is the well's entire production history. Note the jump in production after being taken off-line for a couple of months in late 2016, a year after the original frack. The 5,464 bbls over 4 days extrapolates to 41,000 bbls over a 30-day month. This well continues to flow on its own according to the scout ticket. I follow this well and the other Whiting Flatland Federal wells here.

The well:
  • 30774, 1,844, Whiting, Flatland Federal 11-4-5TFH, t10/15; cum 473K 1/17:
Monthly Production Data

PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN1-201731180271784830726828767976209
BAKKEN12-2016312010219914416184944836101212
BAKKEN11-20163023163237976210775757740658
BAKKEN10-20163135844360841075889424870902217
BAKKEN9-20164546443682234930992753
BAKKEN8-20160000000
BAKKEN7-20161310524107591940465344641471
BAKKEN6-2016302914529290627811279411263648
BAKKEN5-201631347393482370641119211086783136
BAKKEN4-20163037617370834467122637121577960
BAKKEN3-20163144583449235288141867140859903
BAKKEN2-20162443519434479698108313108095142
BAKKEN1-2016315435054271102971340721320611922
BAKKEN12-2015316329363835150051526011479474556
BAKKEN11-201515351583495311139630184968713271
BAKKEN10-201514175281679613243407963029510445

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