Saturday, January 7, 2023

Nice Surprise: An Old EOG Austin Well Has Nice Jump In Production -- January 7, 2023

The "theory" says this is not supposed to happen

The well:

  • 17614, 1,595, EOG, Austin 20-29H, Parshall, t9/09; cum 854K 11/20; off line as of 5/18; back on line as of 11/18; see this post; off line 5/20; back on line 6/20; cum 864K 9/21; cum 875K 11/22; recent production:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN11-202230209820992337768747054
BAKKEN10-202231215121512546716638381
BAKKEN9-202219119311373342590240041
BAKKEN8-2022151551601085634378
BAKKEN7-20223141841714134610940
BAKKEN6-20223050351134154913050
BAKKEN5-202226474464170130311020

No comments:

Post a Comment

Note: Only a member of this blog may post a comment.