Tuesday, November 1, 2022

This Million-Bbl CLR Whitman Well Is Back On Line -- November 1, 2022

The CLR Whitman wells are tracked here.

The well (see also this post):

  • 20212, 482 (1,008 reported on the sundry form), CLR, Whitman 3-34H, Oakdale, Three Forks first bench, API - 33-025-01261; t9/11; cum 181K 5/18; see production profile below; well, isn't this interesting -- yup, this well was fracked 9/23/17 - 10/5/17; 9.8 million gallons of water; 84% water; 15% sand; sundry form in file report: 61 stages; 14.5 million lbs sand; [Update: this well went off line 4/18 and came back on line 8/18; in 8/18 produced 4,731 bbls over 4 days which extrapolates to 35,000 bbls in one month]; interesting profile; see this post; cum 948K 6/21; cum 1,037,348 bbls 1/22; update here; off line while neighboring wells are being fracked ccum 1.059338 million bbls crude oil, 3/22; cum 1.066631 million bbls 9/22.

Recent production: 

PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN9-202221392438206768434340720
BAKKEN8-20227336931832084348734090
BAKKEN7-20220000000
BAKKEN6-20220000000
BAKKEN5-20220000000
BAKKEN4-2022230260254530
BAKKEN3-2022311143411435213524764243520
BAKKEN2-2022281052610625223522769223910
BAKKEN1-2022311172411681304024686242670
BAKKEN12-2021301063010691347322675222820
BAKKEN11-2021301182011842237325132247580
BAKKEN10-2021311326613173234128058276530
BAKKEN9-2021301288912902211526793264100

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