Thursday, September 22, 2022

10X Jump In Production; The Bakken Never Ceases To Amaze Me -- September 22, 2022

The Bakken never ceases to amaze me. Looking for a needle in a haystack, looking for a reason why some great wells were taken off line. Here's the reason:

The well:

  • 35081, 3,556, CLR, Carson Peak 8-35H2, Second Bench Three Forks, 52 stages; 14.2 million lbs; Oakdale, t5/19; cum 116K in 46 days; cum 503K 5/20; cum 685K 7/22; recent production, look at that huge jump in production, noo sundry form to explain jump in production; FracFocus with no data of new frack (which makes sense; new production jump but not high enough to suggest a re-frack):
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN7-20223113552134678332130681286331
BAKKEN6-20228375137332537451444637
BAKKEN5-2022271045104120198467010
BAKKEN4-2022112902946862882200
BAKKEN3-20223110031004191711585470
BAKKEN2-2022281382138617137065690
BAKKEN1-2022311913191025819598050
BAKKEN12-2021301709170930756154700
BAKKEN11-20213022822281399543074056102
BAKKEN10-20212018531857312448364629108

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