Saturday, May 23, 2020

An XTO Lost Bridge Well Goes Over 500K -- May 23, 2020

The well:
  • 19566, 1,971, XTO, Deep Creek 43X-5, Lost Bridge, Bakken, t10/11; cum 504K 3/20; see this note;
Recent production, 16,061 bbls over 15 days extrapolates to 32,122 bbls:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN3-202031256826342400382537770
BAKKEN2-202029259024732060324518251393
BAKKEN1-20203125832708301331597122433
BAKKEN12-20193141314217477256719014744
BAKKEN11-201930571455919560878866722044
BAKKEN10-201919458045927213656928223677
BAKKEN9-20193041594195717962665631583
BAKKEN8-2019317285726587651156980053504
BAKKEN7-201918620061686973943361623222
BAKKEN6-201930532754691038972867008236
BAKKEN5-20193113218129842831122646176414895
BAKKEN4-2019613381852494019851539414
BAKKEN3-201931170051659127559270791683210128
BAKKEN2-2019201137111418168601697593997490
BAKKEN1-20191179107976884813978013913
BAKKEN12-20183127085287653293147742047577
BAKKEN11-201815160611409217397264661232814028
BAKKEN10-20180000000
BAKKEN9-2018003310000
BAKKEN8-201811773960000
BAKKEN7-20180000000
BAKKEN6-20180000000
BAKKEN5-20180000000
BAKKEN4-20180000000
BAKKEN3-2018121264143713522187701225
BAKKEN2-20182436083647647446321812119

No comments:

Post a Comment

Note: Only a member of this blog may post a comment.