Friday, July 26, 2019

Production Jumps 55-Fold; An Old CLR Lansing Well In Banks Oil Field -- July 26, 2019

Production jumps 55-fold, 9,000 bbls over 31 days in 12/18, from 163 bbls over 31 days in 8/18 -- just four months later. The well was originally drilled / fracked back in 2010. This well had a 55-fold jump in production when it was already eight years old. And it will continue to produce for 30 more years.

Another well, a bit further to the west, also showed a jump in production, but it was only a 3-fold jump in production. 

The well:
  • 19126, 76 (no typo), CLR, Lansing 1-25H, Banks, t11/10; cum 412K 5/19;
Recent production:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN5-201927282428392043827479100
BAKKEN4-20193035143402237392088123680
BAKKEN3-20193137823814264284157667330
BAKKEN2-201928315632582471641360520
BAKKEN1-20193142404222346271876548220
BAKKEN12-20183189959124102981067191561105
BAKKEN11-20181233382959866336053308135
BAKKEN10-201810470346145157
BAKKEN9-20183012926573364915292
BAKKEN8-20183116307576752560
BAKKEN7-2018311483236026362170
BAKKEN6-20183013506246202105
BAKKEN5-2018311542907361961960
BAKKEN4-2018282100124080800
BAKKEN3-20180000000
BAKKEN2-20180000000
BAKKEN1-20180000000
BAKKEN12-20170000000
BAKKEN11-201728156716081069462946290
BAKKEN10-201731170319531133536253620

The graphic:

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