Wednesday, March 28, 2018

Put Another Log On The Fire -- Another Bakken Story -- Re-Accomplishing A Failed Frack -- MRO In Bailey Oil Field, #19553 -- March 28, 2018

An example of "saving" a well in the Bakken. 

The well:
  • 19553, 42 (no typo), MRO, Lucy Fleckenstein 34-20H, API - 33-025-01165, Bailey, t5/11; cum 222K 1/18; failed frack in 2011; in 2014, the decision was made to "sidetrack" this well, going down the existing well-bore and punching out at 11,449 feet. This they did, re-fracked with 30 stages and 3.9 million lbs sand, and reported an IP of 2,491 on 2/26/2015. 
  • Note: they re-fracked this well at the same time they fracked a number of wells in the immediate area
Production profile of interest:
BAKKEN9-201530692768894544491619622033
BAKKEN8-20153174177426469756654338352
BAKKEN7-20153166956785429646162984730
BAKKEN6-2015301107810952641264894568566
BAKKEN5-20151458345990479532492302244
BAKKEN4-201530127161258712226881045832686
BAKKEN3-2015311476515758119311659993855454
BAKKEN2-20151118827176565321412736478409
BAKKEN1-20151200000
BAKKEN12-20140000000
BAKKEN11-20140000000
BAKKEN10-2014112340101
BAKKEN9-201428332464483440149
BAKKEN8-201431319228253630143
BAKKEN7-201431328224233680147


Put Another Log On The Fire, Tompall Glaser

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